Minutes Package, July 11, 2016=
ATTENDANCE
Mayor Stephen Molnar
Deputy Mayor Dave Beres Councillor Maxwell Adam
Councillor Penny Esseltine
Councillor Jim Hayes Councillor Chris Rosehart
Councillor Brian Stephenson
Staff:
David Calder, CAO Donna Wilson, Town Clerk Janelle Costantino, Manager of Finance
Rick Cox, Director of Recreation, Culture & Parks Kevin DeLeebeeck, Director of Operations
Jeff Smith, Fire Chief
Tricia Smith, Deputy Clerk
1.Call to Order
The meeting was called to order at 6:00 p.m.
2.Adoption of Agenda
Resolution #1
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT the Agenda as prepared for the Council meeting of Monday, July 11, 2016, be
adopted.
Carried
3.Moment of Silence
The Corporation of the Town of Tillsonburg
COUNCIL MEETING
Monday, July 11, 2016
6:00 PM
Council Chambers
200 Broadway, 2nd Floor
MINUTES
Council Meeting Minutes, July 11, 2016 - 2 -
4.Disclosures of Pecuniary Interest and the General Nature Thereof
There were no disclosures of pecuniary interest declared.
5.Adoption of Council Minutes of Previous Meeting
5.1. Minutes of the Meeting of June 27, 2016
Minutes, June 27, 2016
Resolution #2
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT the Minutes of the Council Meeting of June 27, 2016, be approved.
Carried
6.Delegations and Presentations
6.1. Presentation of the Volunteer Achievement Award - Jack Parker
Presented By: Mayor Molnar and Councillor Stephenson, Special Awards Committee
7.Committee Reports & Presentations
7.1. AIRAC 16-01, Airport Advisory Committee Revised Terms of Reference
Report to Council AIRA C16-01 Airport Advisory Committee Revised
Terms of Reference
AIRAC Revised Terms of Reference 5May2016 (2)
Resolution #3
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT Council receive Report AIRAC 16-01, Airport Advisory Committee Revised
Terms of Reference;
AND THAT Council approve the revised Terms of Reference for the Airport
Advisory Committee.
Carried
Council Meeting Minutes, July 11, 2016 - 3 -
8.Reports from Departments
8.1. Recreation, Culture & Park Services
8.1.1. RCP 16-19, TCC Detailed Engineering Study Report and Recommendations
Delegation By: Ian B. Storey, P. Eng. President, I. B. Storey Inc.
RCP 16-19 TCC Detailed Engineering Study Report and
Recommendations
IB Storey Project Briefing
Tillsonburg Detailed Engineering Study
Resolution #4
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT Council receive Report RCP 16-19, TCC Detailed Engineering
Study Report and Recommendations;
AND THAT Council authorize staff to enter a single-source contract with I.
B. Storey Inc. to develop the system design and RFP specifications for an
energy conservation retrofit at the Tillsonburg Community Centre.
Carried
8.2. Clerk’s Office
8.2.1. CL 16-18, Integrity Commissioner
CL 16-18 Integrity Commissioner
Municipal Act Excerpt S. 223.4 Integrity Commissioner
Resolution #5 was withdrawn.
Option 1 - Do not appoint a Municipal Integrity Official and direct that the
Ontario Ombudsman become the default investigator for the Town of
Tillsonburg.
Council Meeting Minutes, July 11, 2016 - 4 -
Resolution #6
Moved By: Deputy Mayor Beres Seconded By: Councillor Adam
THAT Council receive Report CL 16-18, Integrity Commissioner;
AND THAT Council direct Staff to complete the recommendations
contained in Option 1.
Carried
8.3. Fire and Emergency Services
8.3.1. FRS 16-06, Lucknow & District Fire Communications Contract
FRS 16-06 Fire Communications Lucknow
Lucknow Contract July 2016
Resolution #7
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council receive Report FRS 16-06, Lucknow & District Fire
Communications Contract;
AND THAT the capital costs incurred be debt financed with a term not to
exceed five (5) years;
AND FURTHER THAT Council authorize the Mayor and Clerk to enter into
an agreement with the Lucknow and District Fire Department for the
provision of Fire Dispatch and Communications Services.
Carried
8.4. Operations
8.4.1. OPS 16-21, Results for Tender RFT 2016-007 Hot Mix Asphalt Paving
Program
OPS 16-21 Results for Tender RFT 2016-007 Hot Mix Asphalt Paving
Program
Council Meeting Minutes, July 11, 2016 - 5 -
Resolution #8
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council receive Report OPS 16-21, Results for Tender RFT 2016-
007 Hot Mix Asphalt Paving Program;
AND THAT Council award Tender RFT 2016-007 to Permanent Paving
Ltd. of Woodstock, ON at a cost of $277,046.69 (net HST included), the
lowest bid received satisfying all Tender requirements.
Carried
8.5. Recreation, Culture & Park Services
8.5.1. RCP 16-26, Awarding Purchase of Aquacycles Tender
RCP 16-26 - Awarding Purchase of Aquacycles Tender
RCP 16-03 - OSRCF Application Liquid Gym Initiative
Letter from Ministry of Tourism, Culture & Sport
Resolution #9
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT Council receive Report RCP 16-26, Awarding Purchase of
Aquacycles Tender;
AND THAT Council award the contract to purchase twenty (20)
aquacycles, including three (3) additional accessible seats and three (3)
additional sports seats from Advantage Fitness Sales Inc. (Markham) at a
cost not to exceed their tendered price of $50,891.61 net of applicable
taxes.
Carried
9.Committee Minutes
9.1. Minutes, Cultural Advisory Committee
Minutes, June 1, 2016
9.2. Minutes, Memorial Park Revitalization Sub-Committee
Minutes, June 15, 2016
Council Meeting Minutes, July 11, 2016 - 6 -
9.3. Minutes, Museum Advisory Committee
Minutes, June 23, 2016
9.4. Minutes, Physician Recruitment Committee
Minutes, June 20, 2016
Resolution #10
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT Council receive the Minutes of the Cultural Advisory Committee for June 1,
2016, the Memorial Park Revitalization Sub-Committee for June 15, 2016, the
Museum Advisory Committee for June 23, 2016 and the Physician Recruitment
Committee for June 20, 2016, as information.
Carried
10. Notice of Motions
11. By-Laws
By-Laws from the Meeting of Monday, July 11, 2016
Resolution #11
Moved By: Councillor Adam Seconded By: Councillor Esseltine
11.1. THAT By-Law 4029, To authorize an agreement with the Lucknow and
District Fire Department for the provision of Fire Dispatch and
Communications Services, be read for a first, second and third and final
reading and that the Mayor and the Clerk be and are hereby authorized to
sign the same, and place the corporate seal thereunto.
Carried
Resolution #12
Moved By: Councillor Adam Seconded By: Councillor Esseltine
11.2. THAT By-Law 4030, To confirm the proceedings of Council at its meeting
held on the 11th day of July, 2016, be read for a first, second and third
Council Meeting Minutes, July 11, 2016 - 7 -
and final reading and that the Mayor and the Clerk be and are hereby
authorized to sign the same, and place the corporate seal thereunto.
Carried
12. Items of Public Interest
The Town of Tillsonburg is seeking volunteers for the Canada 150 Sub-Committee,
which will plan a number of Town-wide events in celebration of Canada’s 150th
anniversary of Confederation in 2017. Applications can be submitted on-line at
www.tillsonburg.ca or in person to the Clerk’s Office at 200 Broadway, 2nd Floor,
Tillsonburg, ON.
13. Adjournment
Resolution #13
Moved By: Deputy Mayor Beres Seconded By: Councillor Adam
THAT the Council Meeting of Monday, July 11, 2016 be adjourned at 8:00 p.m.
Carried
Table of Contents
Agenda 2
Minutes, June 27, 2016
Minutes, June 27, 2016 8
Airport Advisory Committee Report 16-01 - Revised Terms of
Reference
Report to Council AAC16-01 Airport Advisory
Committee Revised Terms of Reference 17
AIRAC Revised Terms of Reference 5May2016 (2)18
RCP 16-19 – TCC Detailed Engineering Study Report and
Recommendations
RCP 16-19 ? TCC Detailed Engineering Study Report
and Recommendations 22
IB Storey Project Briefing 24
Tillsonburg Detailed Engineering Study 33
CL 16-18, Integrity Commissioner
CL 16-18 Integrity Commissioner 209
Municipal Act Excerpt S. 223.4 Integrity Commissioner 214
FRS 16-06 Fire Communications Lucknow
FRS 16-06 Fire Communications Lucknow 217
Lucknow Contract July 2016 219
OPS 16-21 Results for Tender RFT 2016-007 Hot Mix Asphalt
Paving Program
OPS 16-21 Results for Tender RFT 2016-007 Hot Mix
Asphalt Paving Program 229
RCP 16-26 – Awarding Purchase of Aquacycles Tender
RCP 16-26 - Awarding Purchase of Aquacycles Tender 233
RCP 16-03 - OSRCF Application ? Liquid Gym Initiative 235
Letter from Ministry of Tourism, Culture & Sport 237
Minutes, Cultural Advisory Committee
Minutes, June 1, 2016 239
Minutes, Memorial Park Revitalization Committee
Minutes, June 27, 2016 241
Minutes, Museum Advisory Committee
Minutes, June 23, 2016 244
Minutes, Physician Recruitment Committee
Minutes, June 20, 2016 247
By-Law 4029, To authorize an agreement with the Lucknow and
District Fire Department for the provision of Fire Dispatch and
Communications Services.
By-Law 4029 250
Agreement 251
By-Law 4030, To confirm the proceedings of Council
By-Law 4030 261
1
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1.Call to Order
2.Adoption of Agenda
Proposed Resolution #1
Moved By:Seconded By:
THAT the Agenda as prepared for the Council meeting of Monday, July 11, 2016, be
adopted.
3.Moment of Silence
4.Disclosures of Pecuniary Interest and the General Nature Thereof
5.Adoption of Council Minutes of Previous Meeting
5.1. Minutes of the Meeting of June 27, 2016
Minutes, June 27, 2016
Proposed Resolution #2
Moved By: Seconded By:
THAT the Minutes of the Council Meeting of June 27, 2016, be approved.
6.Delegations and Presentations
6.1. Presentation of the Volunteer Achievement Award - Jack Parker
Presented By: Mayor Molnar and Councillor Stephenson, Special Awards Committee
The Corporation of the Town of Tillsonburg
COUNCIL MEETING
Monday, July 11, 2016
6:00 PM
Council Chambers
200 Broadway, 2nd Floor
AGENDA
2
Council Meeting – Agenda - 2 -
7.Committee Reports & Presentations
7.1. AIRAC 16-01, Airport Advisory Committee Revised Terms of Reference
Delegation: Euclid Benoit, Chair - Airport Advisory Committee
Report to Council AIRA C16-01 Airport Advisory Committee Revised
Terms of Reference
AIRAC Revised Terms of Reference 5May2016 (2)
Proposed Resolution #3
Moved By: Seconded By:
THAT Council receive Report AIRAC 16-01, Airport Advisory Committee Revised
Terms of Reference;
AND THAT Council approve the revised Terms of Reference for the Airport
Advisory Committee.
8.Reports from Departments
8.1. Recreation, Culture & Park Services
8.1.1. RCP 16-19, TCC Detailed Engineering Study Report and Recommendations
Delegation By: Ian B. Storey, P. Eng. President, I. B. Storey Inc.
RCP 16-19 TCC Detailed Engineering Study Report and
Recommendations
IB Storey Project Briefing
Tillsonburg Detailed Engineering Study
Proposed Resolution #4
Moved By: Seconded By:
THAT Council receive Report RCP 16-19, TCC Detailed Engineering
Study Report and Recommendations;
AND THAT Council authorize staff to enter a single-source contract with
I. B. Storey Inc. to develop the system design and RFP specifications for
an energy conservation retrofit at the Tillsonburg Community Centre.
3
Council Meeting – Agenda - 3 -
8.2. Clerk’s Office
8.2.1. CL 16-18, Integrity Commissioner
CL 16-18 Integrity Commissioner
Municipal Act Excerpt S. 223.4 Integrity Commissioner
Deferred Resolution #5
THAT Council approves the appointment of an Integrity Commissioner;
AND THAT the Town be authorized to issue a Request for Proposal (RFP)
seeking proposals for an Integrity Commissioner, including the
consideration that the appointment be made jointly with the County’s local
municipalities, should they be amenable, and their respective Councils
endorse such an approach;
AND THAT upon Council approval for the appointment of an Integrity
Commissioner, that staff be directed to send copies of Report CL 16-13
and this motion to all Oxford County Municipalities and request that the
local municipality report back to the Town within 30 days from receipt of
this report as to whether they would like to participate and partner with the
Town in the proposed RFP;
AND THAT Staff report back to Council at the August 8, 2016 Council
meeting regarding the status of the appointment of an Integrity
Commissioner.
Proposed Resolution #6
Moved By: Seconded By:
THAT Council receive Report CL 16-18, Integrity Commissioner;
AND THAT Council direct Staff to complete the recommendations
contained in Option 3.
4
Council Meeting – Agenda - 4 -
8.3. Fire and Emergency Services
8.3.1. FRS 16-06, Lucknow & District Fire Communications Contract
FRS 16-06 Fire Communications Lucknow
Lucknow Contract July 2016
Proposed Resolution #7
Moved By: Seconded By:
THAT Council receive Report FRS 16-06, Lucknow & District Fire
Communications Contract;
AND THAT the capital costs incurred be debt financed with a term not to
exceed five (5) years;
AND FURTHER THAT Council authorize the Mayor and Clerk to enter into
an agreement with the Lucknow and District Fire Department for the
provision of Fire Dispatch and Communications Services.
8.4. Operations
8.4.1. OPS 16-21, Results for Tender RFT 2016-007 Hot Mix Asphalt Paving
Program
OPS 16-21 Results for Tender RFT 2016-007 Hot Mix Asphalt Paving
Program
Proposed Resolution #8
Moved By: Seconded By:
THAT Council receive Report OPS 16-21, Results for Tender RFT 2016-
007 Hot Mix Asphalt Paving Program;
AND THAT Council award Tender RFT 2016-007 to Permanent Paving
Ltd. of Woodstock, ON at a cost of $277.046.69 (net HST included), the
lowest bid received satisfying all Tender requirements.
5
Council Meeting – Agenda - 5 -
8.5. Recreation, Culture & Park Services
8.5.1. RCP 16-26, Awarding Purchase of Aquacycles Tender
RCP 16-26 - Awarding Purchase of Aquacycles Tender
RCP 16-03 - OSRCF Application Liquid Gym Initiative
Letter from Ministry of Tourism, Culture & Sport
Proposed Resolution #9
Moved By: Seconded By:
THAT Council receive Report RCP 16-26, Awarding Purchase of
Aquacycles Tender;
AND THAT Council award the contract to purchase 20 aquacycles from
Advantage Fitness Sales Inc. (Markham) at a cost not to exceed their
tendered price of $49,898.22 net of applicable taxes.
9. Committee Minutes
9.1. Minutes, Cultural Advisory Committee
Minutes, June 1, 2016
9.2. Minutes, Memorial Park Revitalization Committee
Minutes, June 27, 2016
9.3. Minutes, Museum Advisory Committee
Minutes, June 23, 2016
9.4. Minutes, Physician Recruitment Committee
Minutes, June 20, 2016
Proposed Resolution #10
Moved By: Seconded By:
THAT Council receive the Minutes of the Cultural Advisory Committee for June 1,
2016, the Memorial Park Revitalization Sub-Committee for June 27, 2016, the
6
Council Meeting – Agenda - 6 -
Museum Advisory Committee for June 23, 2016 and the Physician Recruitment
Committee for June 20, 2016, as information.
10. Notice of Motions
11. By-Laws
By-Laws from the Meeting of Monday, July 11, 2016
Proposed Resolution #11
Moved By: Seconded By:
11.1. THAT By-Law 4029, To authorize an agreement with the Lucknow and
District Fire Department for the provision of Fire Dispatch and
Communications Services, Agreement, be read for a first, second and
third and final reading and that the Mayor and the Clerk be and are hereby
authorized to sign the same, and place the corporate seal thereunto.
Proposed Resolution #12
Moved By: Seconded By:
11.2. THAT By-Law 4030, To confirm the proceedings of Council at its meeting
held on the 11th day of July, 2016, be read for a first, second and third
and final reading and that the Mayor and the Clerk be and are hereby
authorized to sign the same, and place the corporate seal thereunto.
12. Items of Public Interest
13. Adjournment
Proposed Resolution #13
Moved By: Seconded By:
THAT the Council Meeting of Monday, July 11, 2016 be adjourned at _____ p.m.
7
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ATTENDANCE Mayor Stephen Molnar
Councillor Penny Esseltine
Councillor Jim Hayes Councillor Chris Rosehart
Councillor Brian Stephenson Staff:
Donna Wilson, Town Clerk Janelle Costantino, Manager of Finance
Kevin DeLeebeeck, Director of Operations
Corey Hill, Parks & Facilities Manager Tricia Smith, Deputy Clerk
Regrets: Deputy Mayor Dave Beres
Councillor Maxwell Adam David Calder, CAO
1. Call to Order
The meeting was called to order at 6:00 p.m.
2. Adoption of Agenda
Resolution #1
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT the Agenda as prepared for the Council meeting of Monday, June 27, 2016,
be adopted.
Carried
3. Moment of Silence
The Corporation of the Town of Tillsonburg
COUNCIL MEETING
Monday, June 27, 2016
6:00 PM
Council Chambers
200 Broadway, 2nd Floor
MINUTES
8
Council Meeting Minutes, June 27, 2016 - 2 -
4. Disclosures of Pecuniary Interest and the General Nature Thereof
There were no disclosures of pecuniary interest declared.
5. Adoption of Council Minutes of Previous Meeting
5.1. Minutes of the Meeting of June 16, 2016 & June 21, 2016
Minutes, June 16, 2016
Minutes, June 21, 2016
Resolution #2
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT the Minutes of the Council Meeting of June 16, 2016 and the Special
Council Meeting of June 21, 2016, be approved.
Carried
6. Delegations and Presentations
6.1. Presentation of the Volunteer Achievement Award – Ron Bates
Presented By: Mayor Molnar and Matt Scholtz, Special Awards Committee
6.2. T:GO CALL-N-RIDE Update
Delegation By: John Verbakel, CT Pilot Program Steering Committee Chair
John Preston, Community Transportation Coordinator
T:GO Update
Report Update
Ridership Summary
Try T:GO days will be offered on July 17 and August 14 in partnership with
Bethel Pentecostal Church between 8:30 a.m. and 4:30 p.m. and residents can
try the service free of charge.
Residents can book rides on-line at www.ridetgo.ca.
Council requested the Transportation Pilot Program Steering Committee to
include a financial aspect as part of their report to Council in September.
9
Council Meeting Minutes, June 27, 2016 - 3 -
Resolution #3
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT Council receives the delegation regarding the T:GO Call-n-Ride Update,
as information.
Carried
6.3. PW 2016-34 Trans Canada Trail - Work Plan Update
Delegation By: Rob Walton, Director of Public Works, County of Oxford
An application for funding to help offset the cost of fencing along the trail will be
submitted by the County to the Canada 150 program.
PW 2016-34 Trans Canada Trail - Work Plan
Map
Resolution #4
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT Council receive the delegation regarding the Trans Canada Trail Work
Plan Update;
AND THAT the matter be referred during consideration of Agenda item 11.2.2,
RCP 16-25 – TCT Extension Project Work Plan Update.
Carried
Council moved to item 11.2.2 of the agenda.
11. Reports from Departments
11.2 Recreation, Culture & Park Services
11.2.2 RCP 16-25 TCT Extension Project Work Plan Update
RCP 16-25 TCT Extension Project Work Plan Update
10
Council Meeting Minutes, June 27, 2016 - 4 -
Resolution #13
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council receive Report RCP 16-25 TCT Extension Project Work
Plan Update, as information.
Carried
Council resumed the order of business.
7. Committee Reports & Presentations
7.1. CAO 16-08, Town Hall Project Steering Committee Public Notice
Presented By: Marty Klein, Chair Town Hall Project Steering Committee
CAO 16-08
Town Hall Project Letter
Town Hall Public Notice
Resolution #5
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council receive report CAO 16-08 Town Hall Project Steering Committee
Public Notice, as information.
Carried
Resolution #6
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council move into the Committee of Adjustment to hear an application for
Minor Variance at 6:44 p.m.
Carried
8. Public Meetings
8.1. Application for Minor Variance -A-07/16 - Tilldent Holdings, 584 Broadway
A-07/16 Report
Report Attachments
11
Council Meeting Minutes, June 27, 2016 - 5 -
A-07/16 Application
Mr. Eric Gilbert, Development Planner, County of Oxford, appeared before
Council and presented Report A-07/16 for the application for Minor Variance.
Opportunity was given for comments and questions.
The applicant Dan Schinkelshoek appeared in support of the application.
No member of the public appeared in support of or in opposition to the
application.
Resolution #7
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT the Town of Tillsonburg Committee of Adjustment approve Application File
A-07/16, submitted by Tilldent Holdings Limited, for lands described as Lot 7,
Plan 1033, Town of Tillsonburg, municipally known as 584 Broadway, as it
relates to relief from Table 5.24.2.1 – Parking Standards, to decrease the
minimum required parking spaces for a professional office from 37 spaces (1 per
20 m2 of gross floor area) to 36 spaces to facilitate the replacement of an
existing commercial building;
AND THAT approval is conditional upon a building permit for the proposed
medical centre being issued within one year of the date of the Committee’s
decision.
Carried
Resolution #8
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT Council move out of the Committee of Adjustment and move back into
regular session at 6:51 p.m.
Carried
12
Council Meeting Minutes, June 27, 2016 - 6 -
9. Information Items
9.1. Federal Government Review of Public Postal Service
Federal Government Review of Public Postal Service
Council directed staff to post notice of the Federal Government Review of Public
Postal Service and request for public input in the local newspaper and on the
Town website.
Resolution #9
Moved By: Councillor Stephenson Seconded By: Councillor Esseltine
THAT Council receive item 9.1, as information.
Carried
10. Mayor
10.1. MYR 16-08, Update - County of Oxford
MYR 16-08
Resolution #10
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT Council receive Report MYR 16-08, Update County of Oxford, as
information.
Carried
11. Reports from Departments
11.1. Clerk’s Office
11.1.1. CL 16-17, Additional Committee Appointments
Report CL 16-17
Resolution #11
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT Council receive Report CL 16-17, Additional Committee
Appointments;
13
Council Meeting Minutes, June 27, 2016 - 7 -
AND THAT Council appoint Jane Ann McLean and Ken Patterson to the
Memorial Park Revitalization Sub-Committee.
Carried
11.2. Recreation, Culture & Park Services
11.2.1. RCP 16-24 - Green Energy Act Reporting 2016
RCP 16-24 Green Energy Act Reporting 2016
2014 Annual Energy Consumption and GHG Emission Report
Council directed staff to provide a report in the third quarter on the Energy
saving initiatives currently under way in Town facilities in advance of the
2017 budget plan.
Resolution #12
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
THAT Council receive Report RCP 16-24 Green Energy Act Reporting
2016;
AND THAT Council approve the submission of the Energy Consumption
and GHG Emissions report for 2014 to the Province to meet legislated
reporting requirements.
Carried
12. Committee Minutes
12.1. Minutes, Accessibility Advisory Committee
Minutes, June 8, 2016
12.2. Minutes, Development Committee
Minutes, May 10, 2016
12.3. Minutes, Heritage, Beautification & Cemetery Advisory Committee
Minutes, June 2, 2016
12.4. Minutes, Fire Strategic Planning Committee
Minutes, May 31, 2016
14
Council Meeting Minutes, June 27, 2016 - 8 -
12.5. Minutes, Museum Advisory Committee
Minutes, May 26, 2016
12.6. Minutes, Physician Recruitment Committee
Minutes, April 27, 2016
12.7. Minutes, Town Hall Steering Committee
Minutes, April 13, 2016
Minutes, June 9, 2016
Council directed staff to advertise the vacancies on the Museum Advisory
Committee and review the other committees of council to ensure a full
compliment.
Resolution #14
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT Council receive the Minutes of the Accessibility Advisory Committee
for June 8, 2016, the Development Committee of May 10, 2016, the
Heritage, Beautification & Cemetery Advisory Committee for June 2, 2016,
the Fire Strategic Planning Committee for May 31, 2016, the Museum
Advisory Committee for May 26, 2016, the Physician Recruitment
Committee for April 27, 2016, and the Town Hall Steering Committee for
April 13, 2016 and June 9, 2016, as information.
Carried
12.8. Minutes, LPRCA
Minutes, May 4, 2016
Resolution #15
Moved By: Councillor Esseltine Seconded By: Councillor Stephenson
THAT Council receive the minutes from the LPRCA for May 4, 2016 as
information.
Carried
15
Council Meeting Minutes, June 27, 2016 - 9 -
13. Notice of Motions
14. By-Laws
By-Laws from the Meeting of Monday, June 27, 2016
Resolution #16
Moved By: Councillor Hayes Seconded By: Councillor Rosehart
14.1. THAT By-Law 4028, To confirm the proceedings of Council at its meeting
held on the 27th day of June, 2016, be read for a first, second and third
and final reading and that the Mayor and the Clerk be and are hereby
authorized to sign the same, and place the corporate seal thereunto.
Carried
15. Items of Public Interest
On July 1, 2016, a number of events will be taking place throughout the community
including, a Fun Fair on the Lawn event from Noon to 2 p.m. at Annandale National
Historic Site; a wreath laying at the Cenotaph and fireworks at Memorial Park. Visit
www.tillsonburg.ca for more information.
16. Adjournment
Resolution #17
Moved By: Councillor Rosehart Seconded By: Councillor Hayes
THAT the Council Meeting of Monday, June 27, 2016 be adjourned at 7:17 p.m.
Carried
16
Report Title Airport Advisory Committee Revised Terms of
Reference
Report No. AIRAC 16-01
Author Vance Czerwinski, Manager of Public Works on behalf of Euclid Benoit, Airport Advisory Committee Chair
Meeting Type Council Meeting
Council Date July 11, 2016
Attachments Revised Terms of Reference
RECOMMENDATION
THAT Council receive Airport Advisory Committee Report AIRAC 16-01;
AND THAT Council approve the revised Terms of Reference for the Airport Advisory
Committee.
SUMMARY
At the Airport Advisory Committee meeting of May 5, 2016, the committee passed the following
resolution to revise the existing Terms of Reference.
Proposed Resolution #3
Moved By: Geoffrey Lee Seconded By: Rick Lee
THAT the revised Airport Advisory Committee Terms of Reference be accepted
and forwarded to Council for approval.
Carried
The Committee proposes the following changes to the existing Terms of Reference:
• Change the second last bullet in 1.0 Role of the Airport Advisory Committee to more
correctly read: "Advise on aviation matters or initiatives including existing and proposed
regulations by external agencies; and,”
• Change 2.3 to allow the participation of community members as is the current practice:
”The committee should be composed, but not restricted to, members from the following
categories;”
• In 2.3, also delete the third bullet: “Transport Canada, NavCanada or other aviation
agency representative (1)”, as these agencies do not allow their staff to sit on local
advisory committees.
• In 2.3 under Non-Voting members: replace “Development Commissioner” with “Public
Works Manager” as the current practice on the committee.
• Correct numbering of the duplicate “2.3” to “2.4”.
FUNDING IMPACT/ FUNDING SOURCE
There are no financial impacts associated with the proposed change to the Terms of Reference.
Page 1 / 1
17
Airport Advisory Committee
Terms of Reference
Last Revised: May 5, 2016
Mandate
To advise and assist the Town of Tillsonburg on matters pertaining to the Tillsonburg Regional Airport.
The Airport Advisory Committee will provide a forum for receiving input and advice from aviation
stakeholder groups and the community with respect to the Airport Master Plan, strategic initiatives and
operational improvements. The Committee will also provide a forum for dialogue, communication and
education.
1.0 Role of the Airport Advisory Committee
The Airport Advisory Committee will provide input and advice on Airport matters as follows:
x Airport policies including master plan implementation and updates;
x Long term strategies to grow and expand the airport including infrastructure
improvements/expansions and services;
x Opportunities to support the financial self-sufficiency of the airport including increased
revenues and decreased costs;
x Airport awareness including marketing and promotion initiatives;
x Airport initiatives and events;
x Tourism initiatives related to the Airport;
x Advise on aviation matters or initiatives including existing and proposed regulations by external
agencies; and
x Matters referred to the Advisory Committee by Council.
2.0 Organization of the Committee
The Committee shall be composed of people from the Greater Tillsonburg Area/Oxford County who
demonstrate a strong commitment to the terms of reference. A cross selection of people should
attempt to be chosen in order to bring to the committee relevant technical and professional expertise as
well as strong advocacy, communication and organizational skills.
2.1 Appointment will be advertised in local newspapers as per Town’s procedures for Committees of
Council.
2.2 Committee members will be appointed by Council.
2.3 The committee should be composed, but not restricted to, members from the following categories:
x Airport tenants (minimum 2)
x Pilots (minimum 2)
x Town Councillor (1)
x Southwest Oxford Township Councillor (1)
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Non-voting members:
x Public Works Manager
x Airport Administrator
x Oxford County representative
2.4 The term of a Committee Member is four (4) years to coincide with the term of Council.
2.5 A Committee Member may apply for re-appointment for three consecutive terms, in order to
ensure transfer of knowledge and continuity amongst Committee Members.
2.6 One member will be appointed by vote of the Committee at the first meeting of each term to chair
meetings form that term. The Committee will also, at this time, select a Vice-Chair and Secretary for the
same duration.
2.7 A Municipal staff person shall interact in an advisory manner to the committee.
3.0 Meetings
3.1 The Committee will hold a minimum of four (4) quarterly meetings with additional meetings at the
call of the Chair.
3.2 The date and time of the regular meetings will be established at the first meeting of each term.
3.3 Meetings will have a formal agenda.
3.4 Agendas and information packages, that will include the minutes from the previous meeting, will be
sent (via mail, e-mail, or fax) to Committee Members prior to each meeting.
3.5. A majority of Committee Members will constitute quorum for the transaction of business.
4.0 Role of the Chair
The Chair is responsible for ensuring the smooth and effective operation of the Committee and its roles.
This will include responsibility for:
4.1 Calling the meetings to order.
4.2 The Chair is encouraged to create an informal atmosphere to encourage the exchange of ideas such
using a roundtable format.
4.3 Creating an agenda in consultation with the Secretary.
4.4 Chairing the meetings.
4.5 Acting as spokesperson.
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4.6 Representing the Committee on other committees when necessary.
4.7 The Chair shall conduct meetings in accordance with the Town’s Procedural By-law.
4.8 In the absence of the Chair, these responsibilities will be undertaken by the Vice-Chair.
5.0 Role of the Secretary
The Secretary is responsible for ensuring a complete up to date record for the Committee.
5.1 In liaison with the Chair, arrange date, time and venue for meetings.
5.2 In liaison with the Chair, set agendas and circulate to the members two business days prior to the
meeting.
5.3 Circulate draft minutes to the members.
5.4 Keep a complete up to date record on the Committee minutes.
6.0 Role of Members
6.1 Membership on the Committee is a position of responsibility and requires a strong commitment to
the Terms of Reference. Committee members are required to:
6.2 Attend all regular scheduled meetings. Members are required to notify the Chair, Secretary or the
designated municipal staff liaison if they are unable to attend a meeting.
6.3 Review all information supplied to them
6.4 Prepare information for use in the development of materials for the Committee.
6.5 Promote the role of the Committee.
6.6 Offer input to Committee reports to Council.
6.7 Attend training as required to effectively perform their role as a Committee member.
6.8 Committee members are subject to The Municipal Conflict of Interest Act R.S.O, 1990, c.M50 and
must disclose any direct or indirect pecuniary interest. The disclosure must be recorded in the minutes
of the meeting.
7.0 Role of Municipal Staff
The Town of Tillsonburg, by its nature and purpose, affects and is affected by many different Municipal
departments. Assistance will be provided on an as required basis from various departments. Municipal
staff will be responsible for carrying out the following functions with respect to the Committee:
15920
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7.1 Acting as an information resource.
7.2 Orientation of Committee members at the first meeting after Council appointment.
7.3 Assist the Committee in its reporting to Council (see Sec. 8.0).
7.4 Provide correspondence to the Committee.
8.0 Reports to Council
The Committee may advise and make recommendations to Council in accordance with its role. Reports
may be submitted as follows:
8.1 By a Council representative.
8.2 By the Chair or the designated representative.
8.3 Minutes from the Committee meetings.
8.4 Written reports.
An annual report will also be submitted to Council at the beginning of each new year outlining the
Committee’s accomplishments in the previous twelve months.
16021
Report Title TCC DES Report and Recommendations
Report No. RCP 16-19
Author Rick Cox, Director of Recreation, Culture & Parks
Meeting Type Council Meeting
Council Date July 11, 2016
Attachments •IB Storey Project Briefing
•Tillsonburg Detailed Engineering Study
RECOMMENDATION
THAT Report RCP 16-19 – TCC Detailed Engineering Study Report and Recommendations be received for information;
AND THAT Council authorizes staff to enter a single-source contract with I. B. Storey Inc. to
develop the system design and RFP specifications for an energy conservation retrofit at the
Tillsonburg Community Centre.
EXECUTIVE SUMMARY
In 2015, the Town received a grant from the IESO to fund a Detailed Engineering Study (DES) at
the Tillsonburg Community Centre. The DES identified several retrofits that would reduce
energy consumption and for which the funding to implement them could be realized by cost
savings from reduced utility costs. This report presents a summary of the DES and requests
Council approval to proceed to the next step which is the preparation of the system specifications and the RFP documents.
BACKGROUND
The Green Energy Act requires municipalities in Ontario to prepare and implement an Energy
Management Plan. The Town of Tillsonburg’s Energy Management Plan includes actions to identify and implement energy conservation projects that will achieve overall town-wide consumption reductions of 2% per year. The Plan also includes giving consideration to re-
investing the savings from consumption reduction in energy conservation projects.
In the fall of 2015, I. B. Storey Inc. conducted a Detailed Engineering Study (DES) at the
Tillsonburg Community Centre (TCC) to identify system improvements and retrofits that would
have a relatively short return on investment based on available grants, utility cost reductions, lifecycle enhancements and reduced maintenance costs. The cost of the DES was fully funded
by a grant from the IESO through Tillsonburg Hydro Inc. In the DES, the consultants identified 7
measures that could be implemented to save energy and reduce cost. The Briefing Notes
attached to this report summarize the findings of the study. The whole report is also attached
and is available for review from the Corporate Office.
Page 1 / 2 RCP 16-19 TCC Detailed Engineering Stu
22
Now that the report has been completed, staff is seeking approval from Council to proceed with developing detailed specifications and procurement documents to implement the recommended
retrofits in timely manner. Given their familiarity with the TCC and their internationally renowned
expertise in this type of project, in accordance with the Purchasing Policy staff is requesting
Council authorize contracting with I.B. Storey Inc. as a single-source vendor for developing the specifications and tender documents for energy retrofits at the Complex.
CONSULTATION/COMMUNICATION
During the DES process, the consultants worked closely with Town staff to collect data, identify
opportunities and narrow down the preferred options.
Ian B Storey, President of I.B. Storey will be a delegation at the Council meeting to provide detailed commentary on the report his company prepared.
FINANCIAL IMPACT/FUNDING SOURCE
The annual savings in utility and maintenance spending achieved through implementation of the
recommended retrofits at 2016 unit costs is approximately $110,000. Redeploying these
savings to fund the payments on debt incurred for the implementation will have minimal impact on taxation until the debt is paid. Beyond that point, the savings can be redeployed for other
purposes or to fund other capital improvements.
COMMUNITY STRATEGIC PLAN (CSP) IMPACT
Implementing this project contributes to achieving the objective of the Future Oxford
sustainability plan for the County.
Page 2 / 2 RCP 16-19 TCC Detailed Engineering Stu
23
PROJECT
BRIEFING
Town of Tillsonburg
Council Meeting 11 July 2016
Ian B. Storey, P.Eng. – President I.B. Storey Inc.
I.B. Storey Inc.
Ontario Division | 400 Applewood Cres.,
Suite 100 | Vaughan, ON L4K 0C3
T: 416-800-1482 F: 647-438-5707
Briefing Overview
•Pathway to Bundled Solution
•DES Findings
•RE-Bundled Solution
•Recommended Project & Benefit Summary
Detailed
Engineering
Re- Bundle
Re-
Engineer
APPROVAL
Redevelopment
Verified IESO
Funded
Additional
Factors
DES
Pathway to Re-Bundled Project
Specifications
DES Results
OUTSIDE OF DES
Example:
CHALLENGES & OBJECTIVES
Bundled Project Overview
FEATURES
Avoid pending expenses with lifecycle renewal.
The savings are equivalent to the Town
receiving property taxes from 31 new homes1
based on savings today.
Financial
No new funding by reallocating existing
utility spending of over $110,000 annually.
Resolve issue of remote storage of
emergency generator (a potential
emergency issue) in accordance with the
Town’s Emergency Response Plan.
Provision for future outdoor ice rink.
Lifecycle
Emergency
Preparedness
Enhanced
Services
IMPACT
IMPACT
BUNDLED PROJECT
BUNDLED PROJECT
BUNDLED PROJECT
Additional Features & Benefits
Next Steps
Bundle Summary
Avoid pending expenses with lifecycle renewal.
The savings are equivalent to the Town
receiving property taxes from 31 new homes1
based on savings today.
Financial
No new funding by reallocating existing
utility spending of over $110,000 annually.
Resolve issue of remote storage of
emergency generator (a potential
emergency issue) in accordance with the
Town’s Emergency Response Plan.
Provision for future outdoor ice rink.
Lifecycle
Emergency
Preparedness
Enhanced
Services
Charlottetown PE, Canada
Vaughan ON, Canada
902-367-3545 / 416-800-1482
www.ibstorey.ca
info@ibstorey.ca
Tampa, FL USA
Colorado Springs, CO
813-333-7684
www.ibstorey.com
info@ibstorey.com
@IBStoreyInc
Recent Notable Projects
Expert Engineering with NHL Green for various initiatives New York, NY
Expert Engineering for optimization at Amalie Arena Tampa Bay FL and
Rogers Arena Vancouver BC
Expert Rink Engineering – Dallas Stars Organization, Dallas TX
Expert Rink Engineering – Mike Richter’s Rink of Future Project,
Long Island, NY
Expert Redevelopment Engineering – Town of Tillsonburg, ON
<Pending>
I.B. Storey is an independent expert engineering firm specializing
in reallocating existing spending to improve facilities.
From the desk of Ian Storey, P.Eng. Ian Storey, P.Eng
President
I.B. Storey Inc.
T: 416-800-1482 www.ibstorey.ca
Town Council
Town of Tillsonburg
Thank-you for taking the time and consideration during your meeting to review I.B. Storey Inc.’s Project Briefing for the
Tillsonburg Community Centre. The enclosed briefing is founded upon our previous detailed work completed for the
Town of Tillsonburg which outlines the opportunities to achieve lifecycle renewal while further improving the reliability of
the facility for years to come. This project will achieve the Town’s Energy Targets without any new spending required due
to the reallocation of current utility and maintenance expenditures.
Sincerely,
Ian Storey, P.Eng.
Prepared by:
I. B. Storey Inc.
400 Applewood Cres., Suite 100
Vaughan, ON L4K 0C3
Phone: 416-800-1482
Fax: 647-438-5707
Email: info@ibstorey.ca
CONFIDENTIAL & PROPRIETARY
TOWN OF TILLSONBURG COMMUNITY
CENTRE
PROJECT BRIEFING
45 HARDY AVENUE, TILLSONBURG, ONTARIO
JUNE 16, 2016
VERSION 1.0
24
TOWN OF TILLSONBURG
PROJECT BRIEFING
I.B. Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 2 of 5
Professional Energy Solutions Version 1.0
Avoid pending expenses with lifecycle renewal.
The savings are equivalent to the Town
receiving property taxes from 31 new homes1
based on savings today.
BUNDLED PROJECT PIECES
PROJECT FEATURES
BENEFIT SUMMARY
Jumpstart Lifecycle Improvements
Improved Level of Services
Dramatic Cost Reduction by Leveraging
Existing Spending
1Based on current tax rates and 2016 average home
prices in Tillsonburg.
The project bundle will achieve over 4 times the annual
energy consumption reduction goal of 2% as set out in the
Town of Tillsonburg’s Energy Management Plan.
2%
8.5%
0%3%5%8%10%
Target 2%
Project Impact
Further details found in I.B.
Storey DES Report & Refined
Overview of Projects Report
Financial
No new funding by reallocating existing
utility spending of over $110,000 annually.
Resolve issue of remote storage of
emergency generator (a potential
emergency issue) in accordance with the
Town’s Emergency Response Plan.
Provision for future outdoor ice rink.
Lifecycle
Emergency
Preparedness
Enhanced
Services
25
TOWN OF TILLSONBURG
PROJECT BRIEFING
I.B. Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 3 of 5
Professional Energy Solutions Version 1.0
WHAT THIS MEANS FOR THE TOWN OF TILLSONBURG
The recommended approach will allow the Town of Tillsonburg to overcome lifecycle renewal obstacles,
cost hurdles, and the Town of Tillsonburg’s objectives to improve energy stewardship with increased
benefits for local citizens.
PROJECT FINANCIAL SUMMARY
The following table summarizes the project financials with full page screening attached in Appendix A. LifecycleCostTown of Tillsonburg Objectives
Rising Utility Costs
=
Additional Burden
on the Municipality
Reduce Energy Consumption by 1-2 % Annually
Planned Energy Management upgrades to
programs and processes
Mitigate future costs
Improve sustainability
Aging Infrastructure
=
Increased expenses
Project Financial Summary
Cumulative 20-year savings $3,264,0622
Estimated Cost $1,878,000
Return on Investment 9.3%
2 Utility escalation rates are based on historical escalation from 1985.
3 Estimated costs do not include formal contingency
26
TOWN OF TILLSONBURG
PROJECT BRIEFING
I.B. Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 4 of 5
Professional Energy Solutions Version 1.0
August 2016 October
2016 July 2017 August
2017
Global Adjustment Charge
Mitigation
Simplified Model
Additional Global
Adjustment future year
management options may
exist by leveraging project
equipment
SCOPE OF WORK
Based on the previously executed Detailed Engineering Study and Pre-
Redevelopment Findings, the recommended project scope for maximum
value is the following:
New innovative refrigeration system
Integration into existing systems
New pool recovered energy heating circuit
Artificial ice pad conversion “Slapshot Pad”
Pumping improvements for ice and pool operations
Automatic controls upgrades
Pool dehumidifier mechanical system improvements
Backup generator
PROJECT MILESTONES
Key project milestones are illustrated
below with a detailed implementation
schedule attached in Appendix B.
Low Maintenance/ High
Efficiency equipment
Reuse quality existing
equipment
Optimization within pool area
and practice pad for
participant satisfaction
Recycling of existing energy
Backup generator for times of
Emergency
Solution Features
27
TOWN OF TILLSONBURG
PROJECT BRIEFING
I.B. Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 5 of 5
Professional Energy Solutions Version 1.0
Proceed to
Project
Development
Engineering
Proceed to
Project
Authorization
Proceed to
Construction
Environmental
Benefits
Key environmental aspects of
this project include;
Reduce greenhouse gas
emissions of 134 tonnes of
C02
Project impact equivalent to
110 Acres of Forest Annually
Assist County of Oxford in
achieving the objective of
100% Renewable Energy by
2050 as outlined in the
Sustainability Plan
ENERGY PERFORMANCE OUTCOME
NEXT STEPS
COMPANY PROFILE
I.B. STOREY Professional Energy Solutions is an independent speciality engineering firm that focuses on
refrigeration based systems with over 15 years of experience serving recreational, commercial and
industrial sectors across North America. I.B. Storey Inc.’s vast project experience includes engineering
upgrades, specialty engineering, system redevelopment, project facilitation and monitoring and
performance verification engineering. I.B. Storey Inc. has developed a reputation for designing and
implementing innovative, cost effective, and energy efficient systems to maximize a building’s potential.
28
APPENDIX A
D ETAILED FINANCIAL SUMMARY
29
Subject:Date:
GHG Savings Cost of Simple
Opportunity Natural Gas Elec Energy Demand Savings1, 2 per year Project Payback
(ekWh)(kWh) (kW)(t CO2) ($)($)(yr)
Recommended Project: EEM 3, 5, 6 and 7:
-Packaged Refrigeration Plant with Heat Recovery
-Artificial Slapshot Pad and Brine Pump VFD
-Pool Filtration Pump VFD
-Demand Control Ventilation and Pool Dehumidifier
Optimization
-New Backup Generator
$110,199 1,878,000$ 17.0
New Natural Gas Generator Utilization -866,553 323,224 0 -87.4 --
Maintenance Savings as a result of Upgrade ------
TOTALS -128,224 841,413 756 161.7 $110,199 $1,878,000 17.0
NOTES:
1. CO2 equiv. emission factor for energy based on average estimate Reduction
2. Energy Savings per I. B. Storey Inc. Detailed Engineering Study
3. PRELIMINARY Numbers for Financial Illustration Only
Effective Paypack
Total Cost to Owner 1,878,000$
Effective Simple Payback (Yr)17
Savings with utility escalation
Assuming 6.3% Blended Increase from historical
data 3,264,062$
Effective Simple Payback (Yr)10.7
Internal Rate of Return 9.3%
Mechanical Life Expectancy 20 years
Simple Cash Value - End of year 10 1,101,990$
Simple Cash Value - End of year 15 1,652,985$
Internal Rate of Return 3.3%
Environmental Impact
Annual Greenhouse Gas Savings ('t CO2/yr)134
Equivalent Cars Off the Road 27.2
June 9, 2016Detailed Financial Summary
Energy Savings
738,329 518,189 756 249.1
Town of Tillsonburg PROJECT FINANCING SUMMARY I.B. Storey
Professional Energy Solutions CONFIDENTIAL AND PROPRIETARY VER 1.0
30
APPENDIX B
IMPLEMENTATION SCHEDULE
31
ID Task Name Start Finish
Q4 16Q2 16 Q2 17Q3 16 Q1 17
JanNov FebDec Mar MayAugMarAprOctJunJulMay
1 2d 16/08/201615/08/2016Notice to Proceed - Engineering
4w 3d 15/09/201616/08/2016System Design & RFP Document
Preparation
9w 4d 12/05/201707/03/2017Off Site Equipment Construction
2w 1d 04/11/201621/10/2016Contract Preparation
1w 20/10/201614/10/2016Contractor Selection
10w 1d 13/01/201704/11/2016Final Design Configuration
2d 04/04/201703/04/2017Shutdown of Refrigeration Plant
4w 2d 07/07/201708/06/2017Installation of New Systems
4w 2d 08/08/201710/07/2017Completion of Onsite Construction
Duration
Apr Sep
12
6
I.B. Storey Inc.
(902) 367-3545
Charlottetown PE – Vaughan ON
23/08/20172d22/08/2017Construction Complete – Owner Turnover
22/08/20172w 1d08/08/2017Commissioning
10/07/20172d07/07/2017Restart of Refrigeration Plant
07/06/20174d02/06/2017Shipment
3 14/10/20164w 2d15/09/2016RFP Process
2
15
14
13
11
16
17
Town of Tillsonburg
Project Facilitation Project Schedule
10 Lisgar Avenue
Tillsonburg, ON N4G 5A5
519-688-3009
10
8 05/05/201716w 1d13/01/2017Material Order
02/06/20179w03/04/2017Onsite Construction Start (Site Prep)
4
7
9
5 21/10/20162d20/10/2016Contract Award - Contractor
Jun
Q3 17
Jul Aug Sep
32
‐
CONFIDENTIAL & PROPRIETARY
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
45 HARDY AVENUE
TILLSONBURG, ON CANADA
N4G 3W9
VERSION 2.0
DECEMBER 9TH, 2015
Prepared by:
I. B. Storey Inc.
Email: info@ibstorey.ca
Website: www.ibstorey.ca
ATLANTIC OFFICE:
51 University Avenue, Suite 302
Charlottetown, PE C1A 4K8
Phone: 902-367-3545
Fax: 902-367-3546
ONTARIO OFFICE:
400 Applewood Crescent Suite 100
Vaughan, ON L4K 0C3
Phone: 416-800-1482
Fax: 647-438-5707
33
34
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 2 of 56
Professional Energy Solutions Version 2.0
1.0 EXECUTIVE SUMMARY
General
Participant: Town of Tillsonburg
Facility Name: Tillsonburg Community Centre
Study Date: Sep 15th, 2015 to Oct 14th, 2015 (Data Collection)
Oct 12th, 2015 to Oct 26th, 2015 (Analysis)
Description of Project: Identify energy savings measures regarding the configuration
of the community centre ice arena and pool zones.
Contact Name: Rick Cox
Phone: (519) 688‐3009 ext. 4228
E‐mail: rcox@tillsonburg.ca
Consultant’s Information
Company Name: I.B Storey Inc.
Contact Name: Ian Storey, P.Eng
Phone: 416‐800‐1482
Fax: 647‐438‐5707
E‐mail: ian.storey@ibstorey.ca
Measure
Electricity
Savings
Electrical
Demand
Savings
(Peak)
Other
Benefits
[$]
Project
Costs
[$]
Simple
Payback
[years]
Maximum
Incentive
[$]
Project
Payback
[years]
EEM
1
Refrigeration Plant
Controls
Optimization
64,912 kWh
($8,006) ‐ ‐ $25,345 3.2 $12,982 1.5
2
New Refrig. Plant
with Controls
Upgrade
276,120 kWh
($34,056)
810 kW
(68 kW Peak)
($7,717)
$6,92712 $452,805 9.3 $55,224 8.2
3 New Refrig. Plant
with Heat Recovery
278,365 kWh
($34,333)
716 kW
(60 kW Peak)
($6,825)
$23,91012 $960,025 14.8 $55,673 13.9
4
New Refrig Plant
with Heat Recovery
and
Dehumidification
220,781 kWh
($25,901)
322 kW
(27 kW Peak)
($3,067)
$25,57612 $1,290,715 23.1 $42,000 22.3
5
Artificial Slaphot
Pad and Brine Pump
VFD
186,489 kWh
($23,001) ‐ ‐ $92,960 4.0 $37,298 2.4
6 Pool Filtration Pump
VFDs
28,746 kWh
($3,545)
40 kW
(3 kW Peak)
($379)
‐ $20,790 5.3 $5,749 3.8
7
Demand Control
Ventilation and Pool
Dehumidification
Optimization
124,910 kWh
($15,406) ‐ $8,5441 $105,770 4.4 $24,982 3.4
1 Natural Gas Savings
2 Maintenance Savings
35
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 3 of 56
Professional Energy Solutions Version 2.0
Project Summary
Recommended Project Description: Best Financial Value Recommendations
Measures Includes: EEM #2, 5, 6 and 7
Electricity Savings [kWh] (with interactive):515,944 kWh
Electricity Savings [$]: $63,635
Electrical Demand Reduction [kW]: 850 kW (71 kW Peak)
Electrical Demand Reduction [$]: $8,095
Natural Gas Reduction [m3]: 38,019 m3
Natural Gas Reduction [$]: $9,471
Other Net Benefits: $6,000 Maintenance Savings
Total Annual Cost Savings: $87,202
Project Cost [$]: $672,325
Maximum Project Incentive [$]: $54,389
Simple Payback without Incentives [years]:7.7
Simple Payback with Incentives [years]: 7.1
Incremental Payback with Incentives [years]:2.7
36
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 4 of 56
Professional Energy Solutions Version 2.0
TABLE OF CONTENTS
1.0 Executive Summary ......................................................................................................................................... 2
2.0 Base Case ........................................................................................................................................................ 7
2.1 Description of System ..................................................................................................................................... 7
2.1.1 System Type and Area Served ............................................................................................................. 7
2.1.2 Process Flow Diagram - P&ID ............................................................................................................. 8
2.1.3 Equipment Specifications ..................................................................................................................... 9
2.2 Annualized Electricity Consumption ............................................................................................................... 9
2.2.1 Utility Costs ....................................................................................................................................... 10
2.2.2 Annual Operating Hours and System Parameters .............................................................................. 10
2.2.3 Electricity Energy consumption ......................................................................................................... 11
2.2.4 Electrical Demand Breakdown ........................................................................................................... 12
2.2.5 Load Inventory Summary ................................................................................................................... 13
2.2.6 Historical Billing Analysis ................................................................................................................. 14
2.2.7 Compressor Performance and Usage Analysis ................................................................................... 15
2.2.8 Other Measured Equipment Performance and Usage Analysis .......................................................... 18
2.2.9 Facility Load Factor ........................................................................................................................... 27
2.2.10 Overall Baseline Energy Consumption .............................................................................................. 28
3.0 Primary Refrigeration Opportunity Analysis ................................................................................................. 29
3.1 Opportunity Descriptions and Energy Savings .............................................................................................. 29
3.1.1 Refrigeration Plant Controls Optimization ......................................................................................... 29
3.1.2 New Packaged Refrigeration Plant With Control Upgrades .............................................................. 31
3.1.3 New Packaged Refrigeration Plant With Control Upgrades, Heat Recovery And Pool
Dehumidification Upgrades ........................................................................................................................... 33
3.1.4 New Packaged Refrigeration Plant With Control Upgrades, HR, Pool Dehumidification Upgrades
and Arena Dehumidification ......................................................................................................................... 36
3.1.5 Artificial Slapshot Pad and Brine Pump VFD .................................................................................... 39
3.1.6 Pool Filtration Pump VFD ................................................................................................................. 41
3.1.7 Demand Control Ventilation and Pool Dehumidifier Optimization ................................................... 42
3.2 Points of Interest ............................................................................................................................................ 44
3.2.1 Pool Area Air Conditioning to Central Refrigeration plant ................................................................ 44
3.2.2 Pool Dehumidification Using Minimum Outdoor Air, Overcool Reheat with Central A/C
Compressor .................................................................................................................................................... 45
3.2.3 Arena Zone Lighting Upgrade ........................................................................................................... 46
37
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 5 of 56
Professional Energy Solutions Version 2.0
4.0 Opportunity Costs and Payback Periods ........................................................................................................ 47
5.0 Recommendations ......................................................................................................................................... 55
5.1 Payback Analysis ........................................................................................................................................... 55
5.2 Expected Life of implemented Equipment .................................................................................................... 56
5.3 Risks with Performance of Recommended Measures ................................................................................... 56
6.0 Implementation Action Plan .......................................................................................................................... 56
6.1 Project Completion Time ............................................................................................................................... 56
Appendix A – Historical Billing Summary
Appendix B – Drawings and Schematics
Appendix C – Manufacturer Data Sheets
Appendix D – Facility Operating Conditions
Appendix E – Utility Cost Summary
Appendix F – Detailed Scope of Work Documents
Appendix G – Project Schedule
Appendix H – Supporting Documentation
Appendix I – Savings Summary Table
38
TOWN OF TILLSONBURG
DETAILED ENGINEERING STUDY
I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 6 of 56
Professional Energy Solutions Version 2.0
KEY PERSONNEL
Town of Tillsonburg
Rick Cox
Director of Recreation, Culture and Parks
200 Broadway Street
Tillsonburg, ON N4G 5A7
Office: (519) 688‐3009 ext. 4228
Email: rcox@tillsonburg.ca
I.B Storey Inc:
Report Author Technical Team
Colby Cudmore, MScE, E.I.T.Ian Storey, P.Eng, President
I.B Storey Professional Energy Solutions I.B Storey Professional Energy Solutions
400 Applewood Crescent Suite 100 Email: ian.storey@ibstorey.ca
Vaughan, ON L4K 0C3
Phone: 416‐800‐1482 Justin MacDonald, E.I.T.
Fax: 647‐438‐5707 I.B Storey Professional Energy Solutions
Email: justin.macdonald@ibstorey.ca
51 University Avenue, Suite 302
Charlottetown, PE C1A 4K8 Ryan Cooke, E.I.T.
Phone: 902‐367‐3545 I.B Storey Professional Energy Solutions
Fax: 902‐367‐3546 Email: ryan.cooke@ibstorey.ca
Email: colby.cudmore@ibstorey.ca
Joshua Ritchie, E.I.T.
I.B. Storey Professional Energy Solutions
Email: joshua.ritchie@ibstorey.ca
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2.0 BASE CASE
2.1 DESCRIPTION OF SYSTEM
The main system chosen for this study is the ammonia refrigeration system servicing the two ice sheets. The pool
area air handling units and arena air handling units were also investigated as part of this study. The refrigeration
plant consists of three compressors, serving both rinks, totalling 275 HP with a total capacity of 179 TR at average
operating conditions. The facility includes two ice arenas, the Kinsmen Memorial Arena and the Colin Campbell
Community Arena. The Kinsmen Memorial Arena is open from mid‐September to mid‐April each year. In addition
there is a small slapshot pad, which operates in tandem with the Community ice pad. The Tillsonburg Community
Centre also has a 25 meter indoor swimming pool.
An heat recovery ventilation unit (HRV) provides heating, cooling and dehumidification to the pool zone a
continuously running 15 hp supply fan and a 15 hp exhaust fan that cycles on occupancy timer. There is an energy
recovery ventilator (ERV) that serves the pool locker zone with 5 hp supply and exhaust fans that cycle based on an
occupancy timer. These occupancy timers are not properly calibrated. Pool zone cooling is provided by rooftop
condensing units.
The arena zone has two continuously running air handling units with fans providing supply air (7.5 hp) and exhaust
air (5 hp) to two separate zones – the locker and lobby area and the change rooms. The locker and lobby area has
built in cooling provided by a rooftop condensing unit, while the change rooms AHU is not provided with cooling.
The main load on the building is the refrigeration compressors, with three Mycom compressors serving both rinks.
2.1.1 SYSTEM TYPE AND AREA SERVED
The daytime and night time ice temperature set points for the Community rink are 21°F and 22°F, respectively.
Similarly, the daytime and night time ice temperature set points for the Memorial rink are 24.5°F and 25°F,
respectively, with a temperature of 24°F during games. The Community rink does not have a specific temperature
set point for games. The air temperature in the arena zone is maintained at 13°C and 70% relative humidity. Pool
zone temperature set point was 85.5°F with a relative humidity of 50%. Pool zone dehumidifier compressors run
to maintain pool zone temperature conditions as needed. Air handling units serving the arena locker lobby and
changing rooms run continuously, while the exhaust fan serving the pool zone and supply and exhaust fans for the
pool locker area cycle based on an unoccupied setting. Additional pool and auditorium compressors and heaters
operate as needed to maintain zone temperature set points at 18‐20°C.
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2.1.2 PROCESS FLOW DIAGRAM - P&ID
The following diagrams represent high level overviews of the refrigeration systems. Multiple items have been
grouped together for clarity. Larger system schematics can be seen in Appendix B along with the manufacturer’s
data sheets provided in Appendix C.
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2.1.3 EQUIPMENT SPECIFICATIONS
The system chosen for this study is the refrigeration plant. The refrigeration plant consists of three compressors,
serving both rinks, totalling 275 HP with a total capacity of 179 TR at average operating conditions. Refrigeration is
provided to the ice sheets using three (3) shell and tube chillers served by two (2) brine pumps. An underfloor
pump is used to prevent heaving of the ice sheets. Heat is rejected from the building using one (1) Evapco LSCB‐
355 evaporative condenser and associated condenser pump. The following is a summary of the equipment on site:
2.2 ANNUALIZED ELECTRICITY CONSUMPTION
The baseline is an important component of the detailed study; it provides a frame of reference which can be used
to measure energy savings once opportunities are implemented. For the systems of interest, the baselines were
determined using historical log books from the facility, minute interval trending data from the refrigeration control
system from November 2014 to September 2015, daily electrical consumption totals for the metered equipment,
and electrical billing. As well, the metered data was reconciled to 15 minute interval data provided by the LDC
during the time of the assessment period.
Pumps Model
Motor
Nameplate
Rating (HP)
Actual Power
Measurement
(HP)
Rated Conditions Actual Operating Conditions
Brine Pump 1 Armstrong 4030 6x5x10 25.0 27.1 1050 USGPM @ 57 FT H2O 1100 USGPM @ 80 FT H2O
Brine Pump 2 Armstrong 4030 6x5x10 30.0 31.7 1050 USGPM @ 57 FT H2O 1200 USGPM @ 88 FT H2O
Underfloor Pump Armstrong 4030 3x2x8 5.0 2.7 131 USGPM @ 50 FT H2O 150 USGPM @ 48 FT H2O
Pool Filter Pump Pentair Water CHK 50 10.0 8.1 600 USGPM @ 45 FT H2O 400 USGPM @ 66 FT H2O
Totals 70.0 69.5
Condensers Model
Condenser Fan Evapco LSCB-355 25.0 10.2 252 TR @ 96.3°F CT, 20°F
ST, 78°F WBT
Average: 252 TR @ 78°F CT,
5°F ST, 39°F WBT
Condenser Pump Armstrong 4030 6x4x10 15.0 10.8 580 USGPM @ 60 FT H2O 580 USGPM @ 60 FT H2O
Totals 40.0 21.0
Compressor Model
#1 MYCOM N8WB 150.0 138.7 N/A 20.0 psig/133.3 psig
#2 MYCOM N4WB 75.0 57.2 N/A 20.0 psig/133.3 psig
#3 MYCOM N4WA 50.0 30.0 N/A 20.0 psig/133.3 psig
Totals 275.0 226.0
Air Handling Unit
Fans Model
Pool Zone Venmar EnergyPack P18I 30.0 8.4
15,000 CFM Supply,
16,000 CFM Exhaust N/A
Pool Locker Venmar ERV5000i 10.0 9.2
4000 CFM Supply,
5000 CFM Exhaust N/A
Arena Change Room Engineered Air FWA-
173/DJE-60-0-HRW-1500 12.5 9.3
4900 CFM Supply,
5900 CFM Exhaust N/A
Arena Locker Engineered Air FWA-
285/DJ-60-0 12.5 9.3
6500 CFM Supply,
5650 CFM Exhaust N/A
Totals 65.0 36.2
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2.2.1 UTILITY COSTS
The following table provides a breakdown of the electricity costs for the facility.
2.2.2 ANNUAL OPERATING HOURS AND SYSTEM PARAMETERS
The refrigeration plant operates as needed 24/7 all year, with a lower rink load in the late spring and summer
months when only the Colin Campbell Community Arena is in operation. The Kinsmen Memorial Arena is open
from mid‐September to mid‐April each year. In addition there is a small slapshot pad, which operates in tandem
with the Community ice pad. The Tillsonburg Community Centre also has an 25 meter indoor swimming pool which
is open for scheduled activities throughout the year from 6am to 9:30 pm.
Utility Provider
Supply Charge: $0.022 /kWh
Debt Retirement: $0.007 /kWh
Global Adjustment: $0.089 /kWh
Regulatory Charges: $0.006 /kWh
Total Rate: $0.123 /kWh
Service Type: Sub-Transmission Delivery Charge: $9.527 /kW
Electricity
Tillsonburg Hydro
Rate Details
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2.2.3 ELECTRICITY ENERGY CONSUMPTION
The breakdown of the annual electricity consumption of the refrigeration equipment was completed in order to
begin analyzing the energy efficiency measures for the facility. The energy usage breakdown, per category, is
shown below.
Observations and Analysis:
The electricity consumption for the studied equipment for the twelve month period analyzed was 1,403,763
kWh with full facility electricity consumption of 2,488,611 kWh.
The 'Compressors' were the highest consumers of electricity with 40% of the analyzed equipment electricity
consumption and 22% of the full facility electricity consumption. This was reconciled with known run hours as
well as metered data vs. 15 minute total facility interval data to ensure accuracy.
Lighting was the second highest consumer of electricity at the facility with 21% of the facility electricity
consumption, consisting primarily of the arena lighting.
'AHUs and RTUs' was the third largest consumer of electricity at 33% of the analyzed equipment electricity
consumption and 18% of the full facility electricity consumption. This consists rooftop units providing cooling
to the areas surrounding the pool and several supply and exhaust fans.
'Pumps' was the fourth largest consumer of electricity at 22% of the analyzed equipment electricity
consumption and 13% of the full facility electricity consumption. This consists of brine pumps, underfloor
pump and a pool filter pump
‘Condensers’ consisting of the evaporative condenser and its pump made up 5% of the analyzed equipment
electricity consumption and 3% of the full facility electricity consumption.
‘Unmetered RTUs’ made up 5% of the full facility electricity consumption, consisting of RTUs in the pool zone
that were outside of the scope for this project.
'All Other Facility Equipment' makes up the remaining 18% of the electricity consumption at the facility
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2.2.4 ELECTRICAL DEMAND BREAKDOWN
Similarly, the electrical demand drawn by all electricity consuming devices was reconciled against the peak
demand experienced during the studied 2014‐2015 period. The results are presented below.
Observations and Analysis:
The peak electrical demand of the analyzed equipment during the analyzed period analyzed was 416 kW.
'Compressors' had the highest peak demand at 47% of the analyzed equipment peak demand and 34% of the
total facility demand.
'AHUs and RTUs' had the second highest peak demand at 29% of the analyzed equipment peak demand and
21% of the total facility demand.
‘Lighting’ had the third highest peak demand at 20% of the total facility demand.
'Pumps' had 14% of the analyzed equipment peak demand and 10% of the total facility demand.
'Condensers' had 10% of the analyzed equipment peak demand and 7% of the total facility demand.
‘Unmetered RTUs’ had 2% of the total facility peak demand.
'All Other Facility Equipment' makes up the remaining 6% of facility demand.
.
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2.2.5 LOAD INVENTORY SUMMARY
Energy Peak Elec
# Description of Load Group kWh kW %
1 Compressors 560,062 196 40%
2 Pumps 312,493 58 22%
3 Condensers 70,238 40 5%
4 AHUs and RTUs 460,970 122 33%
Facility Totals from Inventory 1,403,763 416
Facility Totals from Bills 2,488,611 583
Electricity Consumption (vs. Full Facility) 56% 71%
Electricity (kWh) Thermal (ekWh) Total (ekWh)
Actual
percentages
Compressors 560,062 560,062 23%
Pumps 312,493 312,493 13%
Condensers 70,238 70,238 3%
AHUs and RTUs 460,970 460,970 19%
Lighting 521,088 521,088 21%
Unmetered RTUs 125,093 125,093 5%
All Other Facility Equipment 438,667 438,667 18%
100%
DATA FOR TOTAL ENERGY BREAKDOWN CHART
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2.2.6 HISTORICAL BILLING ANALYSIS
Observations and Analysis Summary:
Electricity consumption shows a strong seasonal trend with the highest electricity consumption occurring in
September and the lowest in April.
Electrical demand values are elevated July through October, corresponding with an increased cooling load,
with the lowest demand values occurring in the May or June. The peak demand for this facility is generally
associated with activity on the ice sheets.
Load factor is the ratio of the average monthly power demand versus peak monthly demand. This value
depicts a general runtime for equipment throughout the facility. Load factor for this facility is typically around
52%
Apr May Jun Jul Aug Sep Oct Nov Dec Jan Feb Mar Total
Demand kW 523 498 498 572 583 583 568 527 532 532 533 533 6,481
Energy kWh 154,308 166,870 187,128 222,600 221,455 262,435 258,035 215,984 207,942 198,355 178,415 215,084 2,488,6115,144 5,383 6,238 7,181 7,144 8,748 8,324 7,199 6,708 6,399 6,372 6,938 6,818
41% 45% 52% 52% 51% 63% 61% 57% 53% 50% 50% 54%
Natural Gas m
3 23,504 18,551 16,911 22,485 21,720 23,997 23,932 24,152 29,828 38,004 40,128 31,565 314,777
783 598 564 725 701 800 772 805 962 1,226 1,433 1,018 (3 233 eMWh)
189 428 592 584 597 367 303 85 38 2 0 26 3,21022 15 188 233 518 527 803 951 613 0 0 0 3,869
ekWh (Total Energy) 395,698 357,388 360,809 453,518 444,515 508,884 503,813 464,027 514,276 588,661 590,526 539,260 5,721,376
CDD 12 DegreesC
HDD 18 DegreesC
Avg. daily kWh ElectricityLoad Factor
FuelAvg. daily Nat. Gas (m3)
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2.2.7 COMPRESSOR PERFORMANCE AND USAGE ANALYSIS
The following section describes the chiller operation during the metering period. Hourly average power
consumption for the metering period is plotted for each compressor. This information was used in the base case
baseline analysis which forms the basis for the energy efficiency measure calculation.
Observations and Analysis Summary:
Compressor 1 was on for 64% of the metering period providing refrigeration to the ice surface and arena
dehumidification.
The average power draw for compressor 1 was 103.5 kW
On an annual basis Compressor 1 was running for 29% of the time, based on historical log books and trending
data
64%
103.5 kW
86% of peak
Percentage of Time On:
Average Power Demand (When On):
Max Power Demand (When On):
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Observations and Analysis Summary:
Compressor 2 was on for 47% of the metering period providing refrigeration to the ice surface and arena
dehumidification.
The average power draw for compressor 2 was 42.7 kW
On an annual basis Compressor 2 was running for 52% of the time, based on historical log books and trending
data
47%
42.7 kW
85% of peak
Percentage of Time On:
Average Power Demand (When On):
Max Power Demand (When On):
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Observations and Analysis Summary:
Compressor 3 was on for 79% of the metering period providing refrigeration to the ice surface and arena
dehumidification.
The average power draw for compressor 3 was 22.4 kW
On an annual basis Compressor 3 was running for 55% of the time, based on historical log books and trending
data
79%
22.4 kW
87% of peak
Percentage of Time On:
Average Power Demand (When On):
Max Power Demand (When On):
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2.2.8 OTHER MEASURED EQUIPMENT PERFORMANCE AND USAGE ANALYSIS
Observations and Analysis Summary:
Condenser Pump 1 ran for 78% of the metering period, drawing an average of 8.1 kW.
The average Annual duty determined by the tower simulation model utilizing 5 year weather data is 58%
The condenser pump is the first in the condenser sequence, which is an inefficient means of operating the
evaporative condenser. The pump runs without the fan and leads to longer pump run times than necessary
78%
8.1
100%
Percentage of Time On:
Average Power Demand (When On):
Average Power Demand (When On):
VER 2.0
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Observations and Analysis Summary:
Condenser Fan 1 ran for 70% of the metering period, drawing an average of 7.6 kW.
The average Annual duty determined by the tower simulation model utilizing 5 year weather data is 46%
The condenser switches over to dry mode at 34°F outdoor air temperature, after which the fan runs alone
without the pump.
0
2
4
6
8
10
12
Sun Fri Wed Mon Sat Thu Tue SunPower Consumption (kW)Time (Days)
Condenser Fan
70%
7.6
78%
Percentage of Time On:
Average Power Demand (When On):
Average Power Demand (When On):
VER 2.0
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Observations and Analysis Summary:
Cold Brine Pump #1 serving the Memorial Arena was installed with an on/off meter and was found to run for
74% of the metering period.
The Brine pump annual duty was determined by scaling the duty based on the compressor duties to be 46%.
Trending data available on site agrees with this information.
Percentage of Time On: 74%
Average Power Demand (when on): 22.3 kW
Average Power Demand (when on): 100%
VER 2.0
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Observations and Analysis Summary:
Cold Brine Pump #2 serving the Community Arena was installed with an on/off meter and was found to run
for 70% of the metering period.
The Brine pump annual duty was determined by scaling the duty based on the compressor duties to be 65%.
Trending data available on site agrees with this information.
70%
19.8 kW
84%
Percentage of Time On:
Average Power Demand (When On):
Average Power Demand (To Peak):
VER 2.0
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Observations and Analysis Summary:
The pool dehumidification compressors were running for 4% of the metering period with an average power
consumption of 7.0 kW.
The Annual pool dehumidifier compressor consumption based on weather and operation was determined to
be 11%.
Peaks occur when the second compressor in the condensing unit briefly turns on, however for most of the
metering period a single compressor cycles on.
Condenser fans run continuously drawing an average of 0.92 kW.
Percentage of Time On: 4%
Average Power Demand (when on): 7.0 kW
Average Power Demand (when on): 41%
VER 2.0
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Observations and Analysis Summary:
The average power consumption for these rooftop units is 13.6 kW. The peak power draw measured during
the metering period was 41.8 kW.
This meter includes the pool dehumidification condensing unit, three Carrier condensing units serving air
conditioning for lobby and office zones around the pool, and a rooftop unit serving the bathrooms near the
pool zone.
The pool dehumidification unit compressors power consumption has been removed from this graph.
Percentage of Time On: 100%
Average Power Demand (when on): 13.6 kW
Average Power Demand (when on): 32%
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Observations and Analysis Summary:
The average power consumption for these rooftop units is 6.8 kW. The peak power draw measured during the
metering period was 12.6 kW.
This meter includes the supply and exhaust fan for the Pool HRV serving heating, cooling and dehumidification
to the pool zone.
The exhaust fan cycles off periodically based on an unoccupied flag, however this occurs sporadically
throughout the operating hours of the facility and is not consistently controlled leading to a potential for fan
control savings.
Percentage of Time On: 99%
Average Power Demand (when on): 6.8 kW
Average Power Demand (when on): 54%
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Observations and Analysis Summary:
The arena dehumidifier ran continuously throughout the metering period drawing an average of 12.9 kW.
The equipment involved includes the fans and desiccant wheel. Refrigeration is provided by the arena
compressors, and the burner consumption for dehumidifier regeneration was not included.
Percentage of Time On: 100%
Average Power Demand (when on): 12.9 kW
Average Power Demand (when on): 83%
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Observations and Analysis Summary:
The arena dressing room AC unit fans ran continuously throughout the metering period drawing an average of
6.8 kW.
The arena dressing room AC unit compressors did not run during the metering period.
Percentage of Time On: 99%
Average Power Demand (when on): 6.8 kW
Average Power Demand (when on): 92%
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2.2.9 FACILITY LOAD FACTOR
Observations and Analysis Summary:
The average facility load factor is 52% and remains relatively constant with a maximum deviation of 11% in
September and April.
The facility load factor is presented for information purpose only, but it does show that facility operation
remain fairly consistent through the year.
The facility load factor is quite low for this facility, indicating the potential for savings by implementing
demand side management to reduce peak demand levels.
2014 2014 2014 2014 2014 2014 2014 2014 2014 2015 2015 2015
Apr May Jun Jul Aug Sep Oct Nov Dec Jan Feb Mar Total
Billed kW 523 498 498 572 583 583 568 527 532 532 533 533 6,481
Billed kWh 154,308 166,870 187,128 222,600 221,455 262,435 258,035 215,984 207,942 198,355 178,415 215,084 2,488,611
Avg daily kWh 5,144 5,383 6,238 7,181 7,144 8,748 8,324 7,199 6,708 6,399 6,372 6,938 6,818
Load Factor 41% 45% 52% 52% 51% 63% 61% 57% 53% 50% 50% 54%
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2.2.10 OVERALL BASELINE ENERGY CONSUMPTION
Annual compressor consumption was determined from historical log books and trending data downloaded from
CIMCO control system on‐site, with supporting evidence from a proprietary arena energy simulation model. Brine
pump and underfloor pump consumption was determined from 8 months of historical trending data. The Pool
Filter pump energy consumption was determined from metering period extrapolation, as the pump runs
continuously throughout the year. Condenser fan and pump energy consumption was determined from a
calibrated condenser simulation, corroborated with historical log book data. Arena zone dehumidifier, pool
dehumidifier, and arena dressing room AC were determined using outdoor air conditions and equipment
specifications in conjunction with metering data. The remaining pool air handling units were determined using
metering period measurements.
Load Group Description Total kW Total kWh Peak kW
Compressors 168.6 560,062 196
Load Known Unit Total Hours Duty Total Peak kW
Description Qty HP Load Eff'y kW kW kW /Year % kWh Demand
Compressor 1 - Mycom 8A 1 150 88% 95% 103.5 103.500 103.5 8,760 29%258,398 119.9
Compressor 2 - Mycom 4B 1 75 73% 95% 42.7 42.700 42.7 8,760 52%194,133 50.4
Compressor 3 - Mycom 4A 1 50 56% 93% 22.4 22.400 22.4 8,760 55%107,531 25.8
Motor
Load Group Description Total kW Total kWh Peak kW
Pumps 57.9 312,493 58
Load Known Unit Total Hours Duty Total Peak kW
Description Qty HP Load Eff'y kW kW kW /Year % kWh Demand
Brine Pump 1 - Armstrong 4030 6x5x10 1 25 108% 90.2% 22.40 22.400 22.4 8,760 46%90,878 22.4
Brine Pump 2 - Armstrong 4030 6x5x10 1 30 106% 90.2% 26.20 26.200 26.2 8,760 65%148,412 26.2
Underfloor Pump - Armstrong 4030 3x2x8 1 5 54% 86.5% 2.33 2.330 2.3 8,760 63%12,757 2.3
Pool Filter Pump - Pentair Water CHK 50 1 10 81% 86.5% 6.97 6.970 7.0 8,760 99%60,447 7.0
Motor
Load Group Description Total kW Total kWh Peak kW
Condensers 15.7 70,238 40
Load Known Unit Total Hours Duty Total Peak kW
Description Qty HP Load Eff'y kW kW kW /Year % kWh Demand
Condenser Fan #1 - LSCB-355 12538% 92% 7.600 7.600 7.6 8,760 46%30,891 21.7
Condenser Pump - Armstrong 4030 6x4x10 11565% 90% 8.09 8.090 8.1 8,400 58%39,347 18.6
Motor
Load Group Description Total kW Total kWh Peak kWAHUs and RTUs 62.0 460,970 122
Load Known Unit Total Hours Duty Total Peak kW
Description Qty HP Load Eff'y kW kW kW /Year % kWh Demand
Arena Zones - CDI DH-160-12-DSOBBLOCM Dehumidifier Fans 12080% 92% 12.910 12.910 12.9 8,760 100%113,092 15.5Arena Locker Room AC - Engineered Air FWA-285/DJ-60-0 162.515% 92% 7.510 7.510 7.5 8,760 100%65,788 7.5
Arena Change RoomHRU - Engineered Air FWA-173/DJE-60-0-HRW-1500 Fans 112.567% 92% 6.828 6.828 6.8 8,760 100%59,816 8.4
Pool ERV Fans - Venmar ERV5000i 11092% 92% 7.460 7.460 7.5 8,760 57%37,154 15.1Pool HRV Fans - Venmar EnergyPack P18I 13028% 92% 6.810 6.810 6.8 8,760 100%59,656 16.1
Pool Dehumidifier CU - Carrier 38AH-044---101-- Compressor 14022% 92% 6.960 6.960 7.0 8,760 11%6,768 17.1Remaining Pool Area Rooftop Units 16028% 92% 13.550 13.550 13.6 8,760 100%118,698 41.8
Motor
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3.0 PRIMARY REFRIGERATION OPPORTUNITY ANALYSIS
3.1 OPPORTUNITY DESCRIPTIONS AND ENERGY SAVINGS
This section discusses the energy efficiency measures that were identified and provide sufficient savings to warrant
implementation.
3.1.1 REFRIGERATION PLANT CONTROLS OPTIMIZATION
Description of Measure
Currently the average discharge pressure of the refrigeration compressors is 133 psig, however analysis of the
equipment on site indicates that an average discharge pressure of 115 psig should be attainable. By optimizing the
programming of the existing control system and installing controls for the parallel condensing heat exchanger,
additional savings can be realized. A breakdown of the findings is as follows:
Current Operation Observations and Analysis
The refrigeration plant runs 24/7 all year to maintain the Memorial Rink and the Community Rink. The
Community Rink is open all year round and has a practice slap‐shot pad connected to its brine. The Memorial
Rink is open from the middle of September to the middle of April, a seven (7) month operating period.
The three (3) reciprocating ammonia compressors serve three (3) shell and tube chillers, with 22% Calcium
Chloride brine floor cooling the ice sheets.
The one (1) Evaporative condenser provides cooling for the Ammonia plant as well as having a parallel glycol
circuit providing oil cooling. The Condenser currently runs with a high temperature switch over to pump first
operation causing in‐efficient heat rejection capacities.
The Refrigeration plant controller has the ability to utilize ice temperature scheduling, but it is not currently
optimally used to provide recommended temperature set points with its night temperature set point lower
than required.
The current average ammonia plant has a high average discharge pressure of 133 psig, significantly higher
than is necessary for this region.
Recommended Upgrades and Improvements
Reprogram the existing control system to allow compressor condensing pressures as low as 110 psig, in order
to obtain an annual average of 115 psig.
Install sensors and controls on the existing plate and frame condenser to monitor the equipment and ensure it
is operating properly with the reduced head pressure
Optimize the condenser operation to ensure condenser fans and pumps cycle together.
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Professional Energy Solutions Version 2.0
Savings Methodology
Log Book runtimes was used with spot readings to calculate the baseline compressor consumption for both rinks.
Using 5 year weather data the baseline consumption of the current evaporative condensers was calculated based
on the average heat rejection of the existing compressors. The same 5 year weather data was used to find the
consumption of the condenser with the new compressors average heat rejection. The savings were calculated by
adding the existing compressor consumption and the existing condenser consumption and subtracting the
consumptions on the new compressors and the condenser operating with the new heat rejection.
Interactive Effects
EEM 1 cannot be done in conjuction with EEM 2, EEM 3 and EEM 4 as they build on the structure of EEM 1. There
are no interactive effects with EEM 5, EEM 6, or EEM 7.
Software Used
Microsoft Excel
Coolware 8.3.7
Mycom Selection Software
BAC Selection Software
RETscreen Plus
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 64,912 kWh $8,006
Annual Demand Savings: N/A N/A
Interactive Effects: N/A N/A
Maintenance Savings: N/A N/A
Other Benefits: N/A N/A
Overall Savings:64,912 ± 2,142 kWh
64,912 kWh ± 3.3%$8,006 ± $264
Opportunity 1: Refrigeration Plant Controls Optimization
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 31 of 56
Professional Energy Solutions Version 2.0
3.1.2 NEW PACKAGED REFRIGERATION PLANT WITH CONTROL UPGRADES
Description of Measure
Upgrading the existing refrigeration system to a 200 hp refrigeration skid (187TR Nominal), complete with two (2)
Reciprocating Compressors, one (1) Plate and Frame Chiller with suction accumulator, one (1) desuperheater. This
refrigeration plant will have an R6 classification, which does not required the plant to be attended, this upgrade
incorporates refrigeration control optimization; the key findings are summarized below:
Current Operation Observations and Analysis
The refrigeration plant operates as needed 24/7 all year to maintain the Memorial Rink and the Community
Rink.
The Community Rink Ice Sheet (full size 85ft x 185ft) is in service all year round (with a two week shutdown in
July every 2 years for maintenance, the last shutdown was in July, 2015), this ice surface shares a cold brine
distribution system with a practice ‘slap‐shot’ pad (approximately 20’ x 40’).
The Memorial Rink (full NHL size 85ft x 200ft) is open from the middle of September to the middle of April, a
seven (7) month operating period.
The Rinks are cooled using pumped 22% Calcium Chloride brine, which is cooled by three (3) shell and tube
chillers, served by three (3) reciprocating ammonia compressors.
One (1) Evaporative condenser rejects all heat from the Ammonia plant as well as having a parallel glycol
circuit providing compressor oil cooling. The Condenser currently runs with a high temperature switch over to
pump first operation causing in‐efficient heat rejection capacities.
The Refrigeration plant controller has the ability to utilize ice temperature scheduling, but it is not currently
optimally used to provide recommended temperature set points with its night temperature set point lower
than required.
The current average ammonia plant has a high average discharge pressure of 135 psig, discharge pressures in
this area can be maintained at 110PSI, based on local weather data.
Recommended Upgrades and Improvements
Replace three (3) existing reciprocating compressors with two (2) new Mycom M4 compressors (93.5TR Each).
The new compressors shall have common suction and discharge headers and the rinks will be served by a
single plate and frame chiller, this single chiller and suction accumulator will replace the existing three (3) shell
and tube chillers.
The existing pumped glycol oil cooling system and secondary cooling circuit in the evaporative condenser will
be reused.
Reuse the Existing Evaporative condenser and water pumps for the new system.
Reuse the existing brine pumps, with reduced runtimes as a resulting from improved performance.
Install a tank‐style desuperheater to provide heated floodwater at temperatures upto 140°F.
VER 2.0
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Professional Energy Solutions Version 2.0
Savings Methodology
Log Book runtimes were used along with spot readings, and annual trending data from the control system to
calculate the baseline compressor consumption for both rinks. The I.B. Storey Arena model was used to calculate
the consumption of a refrigeration compressor replacement along with an increase in suction temperature. Using
5 year weather data the baseline consumption of the current evaporative condensers was calculated based on the
average heat rejection of the existing compressors. The same 5 year weather data was used to find the
consumption of the condenser with the new compressors average heat rejection. The savings were calculated by
adding the existing compressor consumption and the existing condenser consumption and subtracting the
consumptions on the new compressors and the condenser operating with the new heat rejection. Desuperheater
natural gas savings were determined by discussion on staff to determine the typical floods per day, as well as the
volume of the flood water and temperature. Savings are based on heating the water from city water supply
temperature to 100°F using recovered heat rather than natural gas. The current floodwater temperature is
already aggressive, leading to lower than typical savings for the desuperheater.
Interactive Effects
EEM 2 cannot be done in conjuction with EEM 1, EEM 3 and EEM 4 as they build on the structure of EEM 1. There
are no interactive effects with EEM 5
Software Used
Microsoft Excel
Coolware 8.3.7
Mycom Selection Software
BAC Selection Software
RETscreen Plus
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 276,120 kWh $34,056
Annual Demand Savings: 810 kW $7,717
Natural Gas Savings: 3,722 m3 $927
Interactive Effects: N/A N/A
Maintenance Savings: N/A $6,000
Other Benefits: N/A N/A
Overall Savings:
276,120 ± 3,167 kWh
276,120 kWh ± 1.1%
3,722 m3
$48,700 ± $559
Opportunity 2: Packaged Refrigeration Plant with Controls Upgrade
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3.1.3 NEW PACKAGED REFRIGERATION PLANT WITH CONTROL UPGRADES, HEAT
RECOVERY AND POOL DEHUMIDIFICATION UPGRADES
Description of Measure
Upgrading the existing refrigeration system as described in Section 3.1.2 along with adding a parallel plate and
frame heat recovery condenser to utilize the heat recovered to provide heating to the Pool Zone Air, Central
Lobby, Pool Lounge, pool changerooms, Pool water and Lions Auditorium. Modifications to the Pool Dehumidifier
to allow the mix of return air to reduce the air heating requirements as well as providing better conditioned air
into the pool zone.
Current Operation Observations and Analysis
All the Observations listed in Section 3.1.2 apply for this opportunity.
The Pool zone currently utilizes significant amounts of Natural gas to heat the zone resulting from the air
intake configuration.
o The Pool dehumidifier provides 100% outdoor air ventilation into the pool zone, causing significant
large volumes of air to be dumped into the pool causing excess evaporation and heating
requirements for the system.
The main lobby bathrooms are served by a ducted Rooftop unit that has onboard cooling and electric heating
The Lions Auditorium, Pool Lounge and Central Lobby Air handling units are each served by their own remote
condensing unit for cooling and the pool boiler hydronic loop for heating.
Recommended Upgrades and Improvements
Recommended Upgrades and Improvements from Section 3.1.2 apply for this opportunity
Install a glycol cooled condenser on the refrigeration package which supplies 40% ethylene glycol through the
building via a new piping distribution system
Glycol heating coils will be installed in supply air ducts for the Pool zone air, Pool change rooms, lobby
bathrooms, the main lobby, and the lions auditorium.
One (1) plate and frame glycol heat exchanger will be installed to provide pool water heating
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Professional Energy Solutions Version 2.0
Savings Methodology
Compressor electrical consumption was determined as per section 3.1.2, with additional energy consumption as a
result of operating in heat recovery mode with elevated discharge pressures for part of the year. Facility natural
gas consumption was broken down into base load, associated with constant heating requirements, and weather
dependent consumption for loads that are influenced by outdoor air conditions. Pool heating energy consumption
was determined using known air flow, weather data from Environment Canada, and average zone temperature
and humidity conditions from metering period measurements. A calibrated psychrometrics model was used to
determine the optimized pool energy consumption to target the ideal temperature and relative humidity setpoints
as established by ASHRAE. Additional natural gas savings were found with an hourly heat model for each applicable
zone, taking into account the outdoor air conditions, supply airflow of the air handling unit and the zone
temperature setpoint.
Interactive Effects
EEM 3 depends on EEM 1 and cannot be done in conjuction with it. Due to the nature of the . There are no
interactive effects with EEM 5 or 6. EEM 7 leads to reduced natural gas load in the pool zone which further
enhances the heat recovery potential of this opportunity and improves electrical consumption.
Software Used
Microsoft Excel
Coolware 8.3.7
Mycom Selection Software
BAC Selection Software
RETscreen Plus
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 278,365 kWh $34,333
Annual Demand Savings: 716 kW $6,825
Natural Gas Savings: 71,892 m3 $17,910
Interactive Effects: 8,410 kWh $1,037
11,256 m3 $2,804
Maintenance Savings: N/A $6,000
Other Benefits: N/A N/A
Overall Savings:
286,775 ± 2,355 kWh
286,775 kWh ± 0.8%
83,148 m3
$68,909 ± $291
Opportunity 3: Packaged Refrigeration Plant with Heat Recovery
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Professional Energy Solutions Version 2.0
Sustainability
The equipment required for this opportunity results in a longer payback period than EEM 2 at current energy rates,
and as a result EEM 2 is the recommended project from a purely financial perspective. However, the heat recovery
in use in this opportunity results in a lower overall energy footprint for the building, giving it advantage from the
perspective of sustainability as well as future proofing the facility against the potential of increasing natural gas
costs. An outline of the benefits of this opportunity as well as an analysis of how the incremental payback for this
opportunity over a traditional plant replacement improves with changes in natural gas costs follows:
Lower overall energy footprint than non‐heat recovery plant replacement – additional 671,111 ekWh of total
energy savings
Dramatically reduced greenhouse gas emissions over the non‐heat recovery plant replacement – additional
126 tonnes of CO2 annually
Reduced reliance on natural gas:
o Dangers with natural gas extraction may lead to future volatility in the pricing.
o Increased demand for natural gas in the province as well as changes to the infrastructure required to
deliver natural gas may result in increased pricing
o Opportunity payback is greatly influenced by the natural gas costs, with much improved incremental
paybacks with minor increases to natural gas rates, as the following figure demonstrates
As a result of these considerations, I.B. Storey Inc. believes this opportunity deserves consideration for long term
sustainability of the community centre.
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 36 of 56
Professional Energy Solutions Version 2.0
3.1.4 PACKAGED REFRIGERATION PLANT WITH CONTROL ENHANCEMENTS, HEAT
RECOVERY FOR THE LOBBY, POOL AND ARENA DEHUMIDIFIERS, AND POOL WATER
HEATING (INTEGRATED THERMAL PLANT)
Description of Measure
Upgrading the existing refrigeration system as described in Section 3.1.3 along with adding a second Ammonia
chiller and compressor to provide ‘Air Conditioning’ temperature cooling, at high efficiencies. This measure
involves installing a new cold glycol distribution system supplying coils which serve, the Arena Locker rooms, The
arena dehumidifier, which will be converted to an overcool‐reheat style system. It should be noted that the Air
conditioning plant should also take over cooling for the cooling loads in the pool zone to provide a more robust
integrated cooling system, however due to the paybacks involved is shown as a point of interest for this study.
Current Operation Observations and Analysis
All the Observations listed in Section 3.1.3 apply for this opportunity.
The existing Arena Zone Dehumidifier is a natural gas fired desiccant model with no installed aftercooling coil.
Because there is no aftercooling present in this unit, the dehumidifier delivers warm dry air into both of the
arena zones adding a false refrigeration load onto the ice to after cool the air.
In addition the Arena dehumidifier shares common supply ducting to both arenas, as there are no isolation
dampers in place between the Memorial and Community Rinks.
o This requires that the unit supply dry air to the Memorial rink when its ice sheet is out.
The Arena lobby and locker room Air Handling unit has onboard heating and cooling, and is served using an
onboard condensing unit for cooling and by a natural gas burner for heating.
Recommended Upgrades and Improvements
Recommended Upgrades and Improvements from Section 3.1.3 apply for this opportunity
Re‐automate and modify the existing dehumidifier such that the Desiccant wheel and duct furnace is locked
out under normal operation, and install cold and warm glycol coils such that the unit can be operated as an
overcool reheat dehumidifier.
Install isolation dampers and remote sensors such the correct amount of air (at the appropriate dewpoints)
can be supplied to each rink zone, and isolate the zones when they are out of operation
Install a third reciprocating compressor on the refrigeration package to provide cooling for the new cold glycol
distribution system
Add onto the heat recovery system from Section 3.1.3 the Arena locker room air handling unit and the Arena
Dehumidifier
Implement enhanced control strategies to optimize the operation of all connected equipment including
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o Outdoor air mix optimization for the dehumidifiers (poolzone, and arena), target the dewpoint
setpoint in the mixed air
o Implement an automatic reset on ice temperature schedules, in accordance with IIHF (international
Ice Hockey Federation) recommendations.
o Re‐automate the plant to provide optimal discharge pressure control, relative to outdoor air wetbulb
temperatures.
Savings Methodology
Savings were determined as per EEM #3 described above, with additional considerations for the arena
dehumidification and locker room air conditioning loads. The heating and cooling loads for the arena dehumidifier
were determined with an hourly psychrometrics model, using the outdoor air conditions and unit specifications
and targeting the optimal arena conditions as specified ay the IIHF. The air conditioning load for the dressing room
was found using an hourly model, accounting for the outdoor air conditions and the amount of air entering the
zone.
Interactive Effects
EEM 4 depends on EEM 2 and EEM 3 and cannot be done in conjuction with them. There are no interactive effects
with EEM 5, or 6. EEM 7 leads to reduced natural gas load in the pool zone which further enhances the heat
recovery potential of this opportunity and improves electrical consumption.
Software Used
Microsoft Excel
Coolware 8.3.7
Mycom Selection Software
BAC Selection Software
RETscreen Plus
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 220,781 kWh $27,231
Annual Demand Savings: 322 kW $3,067
Natural Gas Savings: 94,634 m3 $23,576
Interactive Effects: 17,674 kWh $2,180
16,922 m3 $4,216
Maintenance Savings: N/A $2,000
Other Benefits: N/A N/A
Overall Savings:
238,455 ± 1,886 kWh
238,455 kWh ± 0.9%
111,557 m3
$62,269 ± $350
Opportunity 4: Packaged Refrigeration Plant with Heat Recovery with Dehumidification
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Sustainability
As with EEM 3, the equipment required for this opportunity also results in a longer payback period than EEM 2 at
current energy rates, and as a result EEM 2 is the recommended project from a purely financial perspective.
However, this opportunity dramatically reduces the overall energy footprint of the building providing a strong case
for long term sustainability of the community centre and a high resistance to changing energy rates. An outline of
the benefits of this opportunity as well as an analysis of how the incremental payback for this opportunity over a
traditional plant replacement improves with changes in natural gas costs follows:
Full integration provides very low overall energy footprint – additional 419,819 ekWh of total energy savings
over EEM 3 and 1,090,930 ekWh of total energy savings over the financial attractive EEM 2.
Dramatically reduced greenhouse gas emissions over other options – additional 74 tonnes of CO2 annually
over EEM 3 and a total of 197 tonnes of CO2 additional savings over EEM 3.
As with EEM 3, further reduced reliance on natural gas:
o Dangers with natural gas extraction may lead to future volatility in the pricing.
o Increased demand for natural gas in the province as well as changes to the infrastructure required to
deliver natural gas may result in increased pricing
o Opportunity payback is greatly influenced by the natural gas costs, with much improved incremental
paybacks with minor increases to natural gas rates, as the following figure demonstrates
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As a result of these considerations, I.B. Storey Inc. believes this opportunity deserves consideration for long term
sustainability of the community centre.
3.1.5 ARTIFICIAL SLAPSHOT PAD AND BRINE PUMP VFD
Description of Measure
This opportunity involves replacing the existing 20 ft x 40 ft practice ice sheet (Slapshot pad) on the Colin Campbell
Community Arena with a sheet of artificial ice to reduce the cooling load on the arena and enable an ice set point
temperature increase. The artificial ice will reduce the refrigeration load on the compressors and save electricity
on top of the existing improvements.
Current Operation Observations and Analysis
The existing ‘Slapshot Pad’ is a small practice ice sheet (20 ft x 40 ft) that is used for training purposes.
Refrigeration for the slapshot pad is provided off the Colin Campbell Community Arena refrigeration loop, and
the pad receives cooling whenever the main community arena does whether cooling is required or not.
There is no means to control ice thickness in the slapshot pad resulting in a large ice build‐up (up to 6 inches)
by the end of the 2‐year season.
o As a result of the increased thickness slapshot ice pad, the community arena ice sheet temperatures
must be reduce in order to maintain the slapshot pad ice conditions.
Recommended Upgrades and Improvements
Cap off the brine piping leading to the slapshot pad to prevent wasted refrigeration
Install new artificial ice surface to provide a suitable approximation of real ice for practice purposes without
required refrigeration.
Maintain existing air exchange infrastructure to cool the air in the Slapshot Zone using arena air.
Install Variable Frequency Drives (VFDs) on the brine pumps serving the arenas to reduce the flow rate to
compensate for the removal of the slapshot pad. Additional savings can be leveraged by reducing the speed
of the brine pumps to increase the temperature pick up on the brine. A dramatic reduction in pump energy
can be realized by a small change in flow rate.
Reconfigure the automation system to automatically reset the community ice sheet, ice temperature schedule
in accordance with a IIHF recommendations.
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Savings Methodology
Savings were determined using arena refrigeration models to determine the amount of energy saved as a result of
the reduced ice surface area. The model was also used to simulate increasing the ice temperature on the Colin
Campbell Community Arena ice sheet to be in line with IIHF recommendations. The resulting electricity
consumption was compared to the electricity consumption of the current compressor operation to determine
energy savings. Additionally, energy savings associated with decreased brine pump operation due to the reduced
compressor runtime was calculated using the calculated runtime of the compressors following the ice temperature
setpoint change. Brine pump VFD savings were calculated based on pump affinity laws.
Interactive Effects
This opportunity has interactive effects with EEM 2, EEM 3, and EEM 4 as those opportunities already include an
increase in arena ice temperature and reduced brine pump runtimes.
Software Used
Microsoft Excel
Coolware 8.3.7
Mycom Selection Software
BAC Selection Software
RETscreen Plus
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 186,489 kWh $23,001
Annual Demand Savings: N/A N/A
Natural Gas Savings: N/A N/A
Interactive Effects: N/A N/A
Maintenance Savings: N/A N/A
Other Benefits: N/A N/A
Overall Savings:186,489 ± 1,886 kWh
186,489 kWh ± 1% $23,001 ± $350
Opportunity 5: Artificial Slapshot Pad and Brine Pump VFD
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3.1.6 POOL FILTRATION PUMP VFD
Description of Measure
The intent of this opportunity is to install a VFD on the pool filtration pump so they can be slowed down to provide
the target flow rate without throttling, reducing the power consumption of the pumps.
Current Operation Observations and Analysis
Pool Filter pump is designed to provide 600 GPM at 45 feet of head, but flow must be maintained between
400 and 450 GPM to prevent loss of filtration medium.
Pump is currently heavily throttled to provide 400 GPM at 65 feet of head, an inefficient means of flow
control.
Flow rate is controlled based on a flow meter installed nearby.
The filtration pump runs continuously to provide water treatment to the pool.
Recommended Upgrades and Improvements
Install a new inverter duty motor and VFD on the pool filter pump
Reduce the speed of the pump to provide the desired flow rate of 400 GPM
Savings Methodology
Pump affinity laws were used to determine what the new operating speed for the pump would be based on the
current and target pressures. The new power draw of each pump was determined using pump affinity laws, using
the measured power draw of the pumps and the calculated change in speed. Energy savings were determined by
operating the pumps with the calculated power draw for the same duty cycle the pumps currently operate on.
Interactive Effects
There are no interactive effects with this opportunity.
Software Used
Microsoft Excel
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 28,746 kWh $2,614
Annual Demand Savings: 40 kW $350
Interactive Effects: N/A N/A
Maintenance Savings: N/A N/A
Other Benefits: N/A N/A
Overall Savings:28,746 ± 647 kWh
28,746 kWh ± 3.7%$2,964 ± $109
Opportunity 6: Pool Filtration Pump VFD
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3.1.7 DEMAND CONTROL VENTILATION AND POOL DEHUMIDIFIER OPTIMIZATION
Description of Measure
The air handling unit fans serving the arena change room and locker lobby area currently run continuously
regardless of demand. Similarly, the air handling fans for the pool zone and surrounding locker rooms run nearly
continuously with an unusual scheduled unoccupied state that turns off the pool zone exhaust fan and locker room
fans. By installing zone CO2 sensors and operating the fans to ASHRAE minimum standards whenever possible,
only ramping up the fan usage to remove excess CO2, significant fan savings can be realized. Additionally, the pool
zone air handler currently operates with 100% outdoor air intake, resulting in lower than desired humidity levels
and high energy costs (high natural gas costs). Modifications to the Pool Dehumidifier to allow the mix of return
air to reduce the air heating requirements as well as providing better conditioned air into the pool zone.
Current Operation Observations and Analysis
Air handling fans for the pool zone have an erratic "unoccupied" setting that results in the exhaust fan being
turned off sporadically throughout the day.
The air handling fans serving the arena area locker room lobby and change room run continuously regardless
of zone occupancy.
The Pool zone currently utilizes significant amounts of Natural gas to heat the zone due to the air intake
configuration. The Pool dehumidifier puts 100% outdoor air into the pool zone causing significant periods of
the year dry air dumped in the pool causing excess evaporation and heating requirements for the system.
Recommended Upgrades and Improvements
Install CO2 sensors in the pool zone air handler (HRV‐1), the pool locker room air handler (ERV‐1), arena locker
lobby (HRU‐1), and arena change room (HRVD)
Install control systems for the air handling fans in the previously mentioned zones with target CO2 levels and
lockouts for minimum ventilation requirements, in accordance with ASHRAE 62.1 standards (Ventilation for
Acceptable Indoor Air Quality).
Install VFDs on each fan to allow modulation of the ventilation flow rates based on current CO2 requirements
Modify the ducting of the pool dehumidifier to allow for a variable mix of return air and outdoor air to prevent
over‐drying the pool zone air. Operate the mixed air damper to optimize zone humidity using relative
humidity controls.
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Savings Methodology
Schedules of arena and pool zone occupancy were developed using information obtained from operators on site in
conjunction with scheduled pool and arena usage. These schedules were confirmed with metering data for the
poolzone air handler (HRV‐1) and the arena locker room air handler (HRU‐1), to establish a strong baseline which
could be applied to the corresponding air handling units in these zones. For the optimized case, minimum air flow
rates were determined based on ASHRAE requirements, informed by the specifications of each of the rooftop units
and the scheduled occupancy rates. A combination of manufacturer supplied fan curves and affinity laws were
used to determine the annual savings potential for reducing the fans to minimum levels.
Interactive Effects
This opportunity will have interactive savings benefits with EEM #3 and EEM #4, as the reduced energy
consumption of the pool zone heating will lead to enhanced instantaneous electricity savings and natural gas
savings with these opportunities.
Software Used
Microsoft Excel
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 124,910 kWh $15,406
Annual Demand Savings: N/A N/A
Interactive Effects: N/A N/A
Maintenance Savings: N/A N/A
Natural Gas Savings: 34,297 m3 $8,364
Overall Savings:
124,910 ± 2,439 kWh
124,910 kWh ± 2%
34,297 m3
$23,771 ± $464
Opportunity 7: Demand Control Ventilation and Dehumidifier Optimization
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3.2 POINTS OF INTEREST
3.2.1 POOL AREA AIR CONDITIONING TO CENTRAL REFRIGERATION PLANT
Description of Measure
This point of interest involves additional cooling integration for air handling unit loads near the pool zone. Several
air handling units currently provide air conditioning to the offices, lobbies, lounges and various rooms surrounding
the pool area. By installing distribution piping from the new refrigeration plant (EEM #4) the air conditioning load
can be moved to the central refrigeration plant for additional savings.
Current Operation Observations and Analysis
An assortment of 5 rooftop condensing units providing air conditioning to the Lions Auditorium and offices,
lobbies and restrooms surrounding the pool area as well as pool dehumidification.
The existing rooftop units have lower efficiency compared to the new A/C compressor.
Recommended Upgrades and Improvements
Install chilled glycol distribution piping from the new A/C load compressor from EEM #4 to glycol coils installed
in the existing rooftop units serving the area around the pool.
Using existing fans and control systems with newly integrated refrigeration coils to maintain consistency.
Increase the capacity provided to the Lions Auditorium to ensure adequate cooling for the zone.
An estimate of the anticipated savings for this opportunity follows:
79,362 kWh
166 kW
$11,373
$218,300
19.2Incremental Payback
Annual Electricity Savings
Annual Demand Savings
Annual Cost Savings
Install Cost
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 45 of 56
Professional Energy Solutions Version 2.0
3.2.2 POOL DEHUMIDIFICATION USING MINIMUM OUTDOOR AIR, OVERCOOL REHEAT WITH
CENTRAL A/C COMPRESSOR
Description of Measure
This point of interest presents the opportunity to utilize minimum outdoor air introduction and to provide
dehumidification to the pool zone using overcool reheat, with either the existing rooftop condensing unit or the
central plant A/C duty compressor installed with EEM #3. By introducing the minimum OA required by ASHRAE
standards significant natural gas savings can be realized at the cost of a slight electricity penalty over the optimized
schedule recommended in EEM #2. This opportunity has the advantage of dramatically reduced automation
complexity leading to a more robust and reliable approach that may yield greater savings in the long run as the
system continues to operate as intended.
Current Operation Observations and Analysis
Pool dehumidification is primarily accomplished by introducing 100% outdoor air to the space continuously,
leading to a high heating load in the shoulder season and winter months.
Zone tends to be come over dry as a result of low outdoor humidity, leading to increased pool and air
temperatures to compensate for user comfort levels.
Existing dehumidification equipment is rarely used as the incoming outdoor air is typically dryer than required.
Recommended Upgrades and Improvements
Install chilled glycol distribution piping from the new A/C load compressor from EEM #3 to glycol coils installed
in the existing HRV serving the pool zone.
Operate the HRV as an overcool reheat dehumidifier as it currently is to target setpoint conditions.
This option is not recommended currently as the high cost of providing the required field piping is not offset by the
low cost of natural gas presently when compared to the option presented in EEM #2 and EEM #3. However, it may
prove to be a more economical option in the long run. An estimate of the anticipated savings for this opportunity
follows:
699 kWh
263,615 ekWh
205 kW
$6,613
$8,303
$1,690
$52,423
31.0Incremental Payback
Incremental Cost for Cooling Coil
Incremental Savings for Overcool Approach
Demand Savings
Savings with POI‐2 Overcool Reheat Approach
EEM #7 DCV Savings
Electricity Savings
Natural Gas Savings
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 46 of 56
Professional Energy Solutions Version 2.0
3.2.3 ARENA ZONE LIGHTING UPGRADE
Description of Measure
Lighting over the ice sheets in both arenas is currently provided by 1000W metal halide fixtures. Significant energy
savings can be realized by converting these lights to high efficiency LED fixtures. This will lead to both direct
lighting energy usage reductions as well as a reduction of heat load on the ice surface from inefficient lighting. As
an added benefit the LED lights have a long life span with minimal maintenance, leading to additional maintenance
savings over the current metal halide fixtures and the LED bulbs do not suffer from burn in to the same extent.
Spot measurements of the current lighting consumption are needed to determine the accuracy of the savings for
this opportunity within DES standards, and as a result it is included as a point of interest.
Current Operation Observations and Analysis
Kinsmen Memorial Arena lighting is provided by 38 100W metal halide fixtures.
Colin Campbell Community Arena lighting is provided by 21 1000W metal halide fixtures.
Recommended Upgrades and Improvements
Install equivalent LED fixtures on a one to one replacement basis for the 59 1000 W metal halide light fixtures.
Install wireless dimming controls with the lights to ensure desired lighting levels and reduced energy costs
when high light levels are not required.
An estimate of the anticipated savings for this opportunity follows:
Item Savings (kWh) Annual Cost Savings ($)
Annual Electricity Savings: 191,565 kWh $23,627
Annual Demand Savings: N/A N/A
Natural Gas Savings: N/A N/A
Interactive Effects: N/A N/A
Maintenance Savings: N/A $3,200
Other Benefits: N/A N/A
Overall Savings: 191,565 kWh $26,827
POI: Arena Lighting Upgrade
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 47 of 56
Professional Energy Solutions Version 2.0
4.0 OPPORTUNITY COSTS AND PAYBACK PERIODS
EEM #1 ‐ Refrigeration Plant Controls Optimization
Description Units/Hours Unit
Cost Total Cost
Equipment
Relay Panel for Desuperheater & Plate Condenser Control 1 $2,000 $2,000
Temperature Sensors (Plate Condenser Outlet) 1 $820 $820
Remote Zone Sensor (tractor room) 1 $275 $275
Suction Pressure Transducer 1 $1,275 $1,275
Subtotal: $4,370
Pipe, Valves, and Wiring
Sensor Wells, Tap, and Busching 2 $870 $1,740
Subtotal: $1,740
Labour and Misc
Pipefitting labour 8 $120 $960
Automation Programming and Configuration 1 $10,000 $10,000
Updating of As‐Built drawings, and Manuals 1 $2,500 $2,500
Subtotal: $13,460
Demolition
0 $0 $0
0 $0 $0
Subtotal: $0
Sub‐Contracts
Electrical 1 $2,200 $2,200
Shipping and Handling Fees 1 $400 $400
Subtotal: $2,600
Commissioning
Equipment Commissioning 3.0% $22,170 $675
Subtotal: $675
Project Facilitation
10.9% $22,845 $2,500
Subtotal: $2,500
Total Cost $25,345
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Professional Energy Solutions Version 2.0
EEM #2 ‐ Packaged Refrigeration Plant with Control Upgrades
Description Units/Hours Unit
Cost Total Cost
Equipment
Two (2) Mycom M4 Reciprocating Compressors 2 $43,500 $87,000
One (1) Plate and Frame Chiller c/w suction accumulator 1 $103,500 $103,500
One (1) Thermastor Desuperheater 1 $12,350 $12,350
Subtotal: $202,850
Pipe, Valves, and Wiring
8" Steel Elbows for Brine Piping 10 $1,225 $12,250
8" Steel Tees for Brine Piping 6 $1,720 $10,320
8" Butterfly Isolation Valves 6 $1,280 $7,680
8" Sch 40. Steel Brine Piping 80 $80 $6,400
Subtotal: $36,650
Labour and Misc
Installation Labour 804 $120 $96,480
Automation 1 $15,000 $15,000
Contractor Shop Drawings and Detail Configuration 1 $5,000 $5,000
Subtotal: $116,480
Demolition
Removal of in‐plant Piping 1 $12,000 $12,000
Removal and Disposal of Existing Reciprocating Compressors 3 $2,000 $6,000
Removal and Disposal of Existing Shell and Tube Chillers 3 $3,000 $9,000
Subtotal: $27,000
Sub‐Contracts
Electrical 1 $15,000 $15,000
Freight 1 $4,500 $4,500
Hoists and cranes 1 $3,500 $3,500
Permits and Inspections (including TSSA) 1 $1,500 $1,500
Subtotal: $24,500
Commissioning
Equipment Commissioning 1.0% $407,480 $4,075
Subtotal: $4,075
Project Facilitation
10.0% $411,555 $41,250
Subtotal: $41,250
Total Cost $452,805
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 49 of 56
Professional Energy Solutions Version 2.0
EEM #3 ‐ Packaged Refrigeration Plant with Heat Recovery
Description Units/Hours Unit Cost Total Cost
Equipment
One (1) Ammonia Refrigeration Package, Including:
Two (2) Mycom M4 Reciprocating Compressors
1 $292,500 $292,500
One(1) Plate and Frame Chiller c/w suction accumulator
One (1) Plate and Frame Condenser Sized for the Full Heat
Rejection, ‐ Ammonia to Glycol
Two (2) Base Mounted Pumps for Heat Recovery
Circulation, One (1) VFD Equipped
Heat Reclaim Package
One (1) 300 US Gallon Thermal Buffer Tank 1 $10,500 $10,500
Ducted Heating/ Cooling Glycol Coils for Mandated AHU's 5 $5,000 $25,000
Pool Preheat Exchanger 1 $22,500 $22,500
Duct Humidity Sensors 3 $870 $2,610
Duct Temperature Sensors 8 $515 $4,120
Rooftop Upblast Exhaust Fan 1 $12,500 $12,500
VFD for Roof Exhaust Fan 1 $7,000 $7,000
Subtotal: $376,730
Pipe, Valves, and Wiring
6" Sch. 80 PVC HR Glycol Piping c/w Insulation 1250 $60 $75,000
6" Butterfly Isolation Valves, Lever Actuator 16 $925 $14,800
6" Sch. 80 PVC Elbows 30 $325 $9,750
6" Sch. 80 PVC Tees 28 $325 $9,100
3" Reducing Couplings 12 $745 $8,940
3" Butterfly Solenoids 6 $1,025 $6,150
3" Sch. 80 PVC HR Glycol Piping c/w Insulation 360 $15 $5,400
Galvanized Steel Ducting (lbs) 2500 $3 $6,875
Subtotal: $136,015
Labour and Misc
Equipment Installation 940 $120 $112,800
Glycol Pipefitting 968 $120 $116,160
Sheetmetal Contractor 116 $120 $13,920
Automation Programming 1 $15,000 $15,000
Shop Drawings, Proofing, Piping and Layout Schematics 1 $7,500 $7,500
Subtotal: $265,380
Demolition
Removal of in‐plant Piping 1 $12,000 $12,000
Removal and Disposal of Existing Reciprocating Compressors 3 $2,000 $6,000
Removal and Disposal of Existing Shell and Tube Chillers 3 $3,000 $9,000
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Professional Energy Solutions Version 2.0
Subtotal: $27,000
Sub‐Contracts
Electrical 1 $35,000 $35,000
Hoists and cranes 1 $12,500 $12,500
Freight 1 $9,500 $9,500
Permits and Inspections 1 $2,000 $2,000
Subtotal: $59,000
Commissioning
Equipment Commissioning 1.0% $864,125 $8,650
Subtotal: $8,650
Project Facilitation
10.0% $872,775 $87,250
Subtotal: $87,250
Total Cost $960,025
EEM #4 ‐ Packaged Refrigeration Plant with Heat Recovery for Dehumidification
Description Units/Hours Unit Cost Total Cost
Equipment
One (1) Ammonia Refrigeration Package, Including:
Three (3) Mycom M4 Reciprocating Compressors
1 $438,000 $438,000
Two(2) Plate and Frame Chillers c/w suction accumulators
One (1) Plate and Frame Condenser Sized for the Full Heat
Rejection, ‐ Ammonia to Glycol
Two (2) Base Mounted Pumps for Heat Recovery Circulation, One
(1) VFD Equipped
Cooling Equipment for Arena Dehumidifier and Lobby A/C unit
Glycol Feeder System 1 $1,225 $1,225
Expansion Tank 1 $5,225 $5,225
Cold Glycol Coils 2 $5,000 $10,000
Heat Reclaim Package
300 US Gallon Thermal Buffer Tank 1 $10,500 $10,500
Ducted Heating Glycol Coils for Mandated AHU's 6 $5,000 $30,000
Pool Preheat Exchanger 1 $22,500 $22,500
Duct Humidity Sensors 3 $870 $2,610
Duct Temperature Sensors 9 $515 $4,635
Rooftop Upblast Exhaust Fan 1 $12,500 $12,500
VFD for Roof Exhaust Fan 1 $7,000 $7,000
Subtotal: $544,195
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Professional Energy Solutions Version 2.0
Pipe, Valves, and Wiring
6" Sch. 80 PVC HR Glycol Piping 1250 $60 $75,000
6" Butterfly Isolation Valves, Lever Actuator 18 $925 $16,650
6" Sch. 80 PVC Elbows 30 $325 $9,750
6" Sch. 80 PVC Tees 32 $325 $10,400
4" Sch. 80 PVC Cold Glycol Piping 300 $25 $7,500
4" Butterfly Isolation Valves, Lever Actuator 8 $575 $4,600
4" Sch. 80 PVC Elbows 12 $165 $1,980
3" Reducing Couplings 14 $745 $10,430
3" Butterfly Solenoids 7 $1,025 $7,175
3" Sch. 80 PVC HR Glycol Piping 420 $15 $6,300
Galvanized Steel Ducting (lbs) 4000 $3 $11,000
Subtotal: $160,785
Labour and Misc
Equipment Installation 1,360 $120 $163,200
Glycol Pipefitting 1,124 $120 $134,880
Sheetmetal Contractor 184 $120 $22,080
Automation Programming 1 $15,000 $15,000
Shop Drawings, Proofing, Piping and Layout Schematics 1 $7,500 $7,500
Subtotal: $342,660
Demolition
Removal of in‐plant Piping 1 $12,000 $12,000
Removal and Disposal of Existing Reciprocating Compressors 3 $2,000 $6,000
Removal and Disposal of Existing Shell and Tube Chillers 3 $3,000 $9,000
Subtotal: $27,000
Sub‐Contracts
Electrical 1 $45,000 $45,000
Hoists and cranes 1 $15,000 $15,000
Insulation 1 $15,200 $15,200
Freight 1 $10,000 $10,000
Permits and Inspections 1 $2,000 $2,000
Subtotal: $87,200
Commissioning
Equipment Commissioning 1.0% $1,161,840 $11,625
Subtotal: $11,625
Project Facilitation
10.0% $1,173,465 $117,250
Subtotal: $117,250
Total Cost $1,290,715
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I.B.Storey Inc. CONFIDENTIAL & PROPRIETARY PAGE 52 of 56
Professional Energy Solutions Version 2.0
EEM #5 ‐ Artificial Slapshot Pad and Brine Pump VFD
Description Units/Hours Unit
Cost Total Cost
Equipment
Artificial Ice Sheet Materials for Slapshot Pad 1 $18,500 $18,500
30HP Brine Pump VFD ‐ Community Pad 1 $13,500 $13,500
30HP Inverter Duty Motor 1 $3,300 $3,300
25HP Brine Pump VFD ‐ Community Pad 1 $10,750 $10,750
25HP Inverter Duty Motor 1 $2,900 $2,900
Subtotal: $48,950
Pipe, Valves, and Wiring
Motor Feeder Wiring 60 $10 $600
Subtotal: $600
Labour and Misc
Installation Labour for Ice Sheet 78 $120 $9,360
Automation Programming and Configuration 1 $2,500 $2,500
Subtotal: $11,860
Demolition
Removal and Disposal of Existing Motors and Wiring 2 $350 $700
0 $0 $0
Subtotal: $700
Sub‐Contracts
Concrete (for levelling floor and crackfilling) 1 $3,000 $3,000
Electrical Subcontract 1 $15,750 $15,750
Freight 1 $1,200 $1,200
Subtotal: $19,950
Commissioning
Equipment Commissioning 3.0% $82,060 $2,450
Subtotal: $2,450
Project Facilitation
10.0% $84,510 $8,450
Subtotal: $8,450
Total Cost $92,960
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Professional Energy Solutions Version 2.0
EEM #6 ‐ Pool Pump VFD
Description Units/Hours Unit
Cost Total Cost
Equipment
10 HP VFD for Pool Filtration Pump 1 $3,200 $3,200
10 HP Inverter Duty Motor 1 $1,350 $1,350
Turbidity Sensor 1 $2,150 $2,150
Unitary PLC Controller (networkable) 1 $2,500 $2,500
Subtotal: $6,700
Pipe, Valves, and Wiring
Sensor Wells, Tap, and Busching 1 $870 $870
Motor Feeder Wiring 60 $10 $600
Subtotal: $1,470
Labour and Misc
Pipefitting labour 26 $120 $3,120
Automation Programming and Configuration 1 $1,500 $1,500
Subtotal: $4,620
Demolition
Removal and Disposal of Existing Motor and Wiring 1 $350 $350
0 $0 $0
Subtotal: $350
Sub‐Contracts
Electrical 1 $4,400 $4,400
Freight 1 $800 $800
Subtotal: $5,200
Commissioning
Equipment Commissioning 3.0% $18,340 $550
Subtotal: $550
Project Facilitation
10.0% $18,890 $1,900
Subtotal: $1,900
Total Cost $20,790
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Professional Energy Solutions Version 2.0
EEM #7 ‐ Demand Control Ventilation
Description Units/Hours Unit
Cost Total Cost
Equipment
Unitary Programmable (networked) DDC controllers with
Touchscreen Display 4 $2,000 $8,000
15 HP VFD's for Pool HRV Supply and Return Fans 2 $4,215 $8,430
15 HP Inverter Duty Motors 2 $1,950 $3,900
5 HP VFD's for Pool Dressing Room ERV Supply and Return
Fans 2 $2,515 $5,030
5 HP Inverter Duty Motors 2 $900 $1,800
7.5 HP VFD's for Pool Dressing Room HRU‐1 and HRVE Supply
Fans 2 $2,940 $5,880
7.5 HP Inverter Duty Motors 2 $1,150 $2,300
5 HP VFD's for Pool Dressing Room HRU‐1 and HRVE Return
Fans 2 $2,515 $5,030
5 HP Inverter Duty Motors 2 $900 $1,800
Duct CO2 Concentration Sensor 4 $850 $3,400
Subtotal: $45,570
Pipe, Valves, and Wiring
Motor Feeder Wiring 400 $10 $4,000
Subtotal: $4,000
Labour and Misc
Automation Programming and Configuration 1 $12,500 $12,500
Shop Drawings, Schematics, and Manuals 1 $2,500 $2,500
Subtotal: $15,000
Demolition
Removal and Disposal of Existing Motor and Wiring 8 $350 $2,800
Subtotal: $2,800
Sub‐Contracts
Electrical 1 $21,000 $21,000
Shipping and Handling Fees 1 $3,500 $3,500
Hoists, Cranes, and lifts 1 $1,500 $1,500
Subtotal: $26,000
Commissioning
Equipment Commissioning 3.0% $93,370 $2,800
Subtotal: $2,800
Project Facilitation
10.0% $96,170 $9,600
Subtotal: $9,600
Total Cost $105,770
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Professional Energy Solutions Version 2.0
5.0 RECOMMENDATIONS
Based on discussions with Town of Tillsonburg regarding the identified energy efficiency measures and the
calculated energy savings it is recommended that following energy efficiency measures be implemented:
5.1 PAYBACK ANALYSIS
This section provides the results of the overall project savings in terms of a Simple Payback (no incentives) and a
Project Payback (maximum incentives). Note that these results are different than the paybacks shown in Section
4.0 as the interactive effects are shown in the following table. Utilizing both Section 4.0 and 5.1 provides the ability
to analyze individual projects as well as the overall recommended project with interactive effects.
Subject Date:October 30, 2015 By I.B Storey Inc.Date:1 of 1
Natural Gas Electric Demand GHG Natural Gas Maintenance Electric
ekWh kWh kW tCO2 $$$ Years Years Yes/No
1 0 64,912 0 14 $0 $0 $8,006 N/A N/A $25,345 3.2 No
2 38,225 276,120 810 68 $927 $6,000 $41,773 $67,830 1.4 $452,805 9.3 Yes
3 738,329 278,365 716 196 $17,910 $6,000 $41,158 $575,050 8.8 $960,025 14.8 No
4 971,894 220,781 322 226 $23,576 $2,000 $30,298 $905,740 16.2 $1,290,715 23.1 No
5 0 186,489 0 41 $0 $0 $23,001 N/A N/A $92,960 4.0 Yes
6 Pool Filtration Pump VFD 0 28,746 40 6 $0 $0 $3,924 N/A N/A $20,790 5.3 Yes
7 352,232 124,910 0 92 $8,544 $0 $15,406 N/A N/A $105,770 4.4 Yes
POI 3 0 191,565 621 42 $0 $0 $29,540 N/A N/A $133,400 4.5 No
Natural Gas Electric Demand GHG Natural Gas Maintenance Electric
ekWh kWh kW tCO2 $$$Years
390,457 515,944 850 207 $9,471 $6,000 $71,731 $672,325 7.7
Natural Gas Electric Electric Natural Gas Maintenance
ekWh kWh $ $ $ $ $
390,457 515,944 $71,731 $9,471 $6,000 $672,325 $54,389
$87,202
1. The maximum incentive shown has the Detailed Engineering Study incentive removed.2. Payback periods are based on current installation costs and the most recent energy lates. Escalating energy costs may lead to reduced payback periods, while a delay in constructioncould result in longer paybacks as construction costs increase over time.
Refrigeration Plant Controls Optimization
Demand Control Ventilation and Pool Dehumidifer Optimization
Recommended Energy Project: EEM# 2,5,6,7
Recommended Energy Project: EEM# 1
Packaged Refrigeration Plant with Control Upgrades
Recommended Energy Project
The following table represents the combined annual savings for the overall project. Values given in the following table represent the savings for implementing together, thus interactive effects are incorporated.
OPPORTUNITY DESCRIPTION ESTIMATED
COST
SIMPLE PAYBACKANNUAL SAVINGS
7.1
Packaged Refrigeration Plant with Heat Recovery
Packaged Refrigeration Plant with Heat Recovery for DehumidificationArtificial Slapshot Pad and Brine Pump VFD
Arena Lighting Upgrade to LEDs
Notes:
OPPORTUNITY DESCRIPTION
PROJECT COST MAXIMUM INCENTIVE
PROJECT PAYBACK
(with Incentives)
Years
ANNUAL SAVINGS
Total Annual Cost Savings
Savings Summary Table
ANNUAL SAVINGS ANNUAL COST SAVINGS
Tillsonburg Community Centre, Tillsonburg, ON
Opportunity Savings
Values given in the following table represent the savings for implementing each individual opportunity against current operating conditions. Savings for some measures, if implemented together, are interrelated.
Interrelation refers to combining opportunities that may have a positive or negative financial impact on each respective opportunity. These interactive effects are not included in this table.
OPPORTUNITY DESCRIPTION
INCREMENTAL
PROJECT COST
INCREMENTA
L PAYBACK
Include in Overall
Project?PROJECT COST
SIMPLE
PAYBACK
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Professional Energy Solutions Version 2.0
5.2 EXPECTED LIFE OF IMPLEMENTED EQUIPMENT
The Original Refrigeration plant was installed in 1972 with a second ice rink constructed in 1977. Additional
refurbishments added a third compressor (Compressor) in 2004. All of the current compressors are expected to
have a useful life exceeding 10 years. The condenser and chillers are expected to have useful lives exceeding 10
years. Condenser pump is expected to have a useful life exceeding 10 years with regular maintenance. If any of the
above equipment malfunctions, or becomes in need of repair, the town of Tillsonburg intends to repair the
affected equipment to the same conditions.
5.3 RISKS WITH PERFORMANCE OF RECOMMENDED MEASURES
Equipment operation may fall outside of standard operating parameters. In other words, the performance of the
equipment is based on manufacturer’s specifications and/or performance data. Therefore, the measures are based
off of rated performance – if the equipment does not operate at these conditions due to improper maintenance,
tune ups, manual intervention, control strategies, project commissioning, etc. then the energy efficient measures
will still work effectively but not necessarily as predicted in the savings calculations.
6.0 IMPLEMENTATION ACTION PLAN
The proposed energy efficiency measures are accompanied by Detailed Scopes of Work as provided in Appendix F.
Since this is an operating recreation facility proper sequencing of the implementation must be done to ensure that
minimal down time of services will occur. This may require performing some installations during the weekend or
during times of lower production demands to ensure that the system can sustain the refrigeration demands. This is
to be coordinated by the successful contractor and Town of Tillsonburg
6.1 PROJECT COMPLETION TIME
Expected project completion dates and schedules for the proposed measure are shown in Appendix G. Potential
project timeline risks include:
High Usage Demands – if the facility requires specific usage demands during the intended construction
period (i.e. scheduled tournaments) certain measures may need to be delayed until the usage demands
diminish. Consultation between the contractor and Town of Tillsonburg. will be required, as well as
proper planning, to guard against this situation.
Construction time overruns – if the implementation of the energy efficiency measure takes longer than
planned, then aside from incremental time overruns, the allotted time to implement may close until
another drop in production occurs.
Permits – since some of these measures involve replacing/modifying existing ammonia piping, proper
permits will be required to comply with all applicable regulations.
VER 2.0
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Tillsonburg Community Centre, Tillsonburg, ONHistorical Billing Analysis - 2014-2015AprMayJun JulAug Sep Oct NovDec Jan Feb MarTotalDemand kW 523 498 498 572 583583 568 527 532 532 533 5336,481Energy kWh154,308 166,870 187,128 222,600 221,455 262,435 258,035 215,984 207,942 198,355 178,415 215,0842,488,6115,144 5,383 6,238 7,181 7,144 8,748 8,324 7,199 6,708 6,399 6,372 6,9386,81841% 45% 52% 52% 51% 63% 61% 57% 53% 50% 50% 54%Natural Gasm323,504 18,551 16,911 22,485 21,720 23,997 23,932 24,152 29,828 38,004 40,128 31,565314,777783 598 564 725 701 800 772 805 962 1,226 1,433 1,018(3 233 eMWh)196 428 592 584 597494 311 853920263,352221562 225 518526 806 951 6130003,737ekWh (Total Energy)395,698 357,388 360,809 453,518 444,515 508,884 503,813 464,027 514,276 588,661 590,526 539,260 5,721,376CDD 12 DegreesCHDD 18 DegreesCAvg. daily kWh ElectricityLoad FactorFuelAvg. daily Nat. Gas (m3)0100200300400500600050,000100,000150,000200,000250,000300,000Average Daily Consumption (kWh) ElectricityCDD0100200300400500600700Peak Monthly Billing Demand (kW)I.B. Storey Inc.Professional Energy Solutions- CONFIDENTIAL AND PROPRIETARY -Ver 1.00100050,0000100All Other Equipment44%Metered System(s)56%Total Energy (% ekWh)0%10%20%30%40%50%60%70%80%90%100%Load Factor (%) I.B. Storey Inc.Professional Energy Solutions- CONFIDENTIAL AND PROPRIETARY -Ver 1.091
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5A4BC321DATEDEDRAWING NUMBERSHEET NO.5CREVISIONSHEET SIZECHECKED BYDRAWN BYPROJECTCLIENT432ABCREVISIONSDDATEEBYSTAMPNOTES51 UNIVERSITY AVENUE, SUITE 302CHARLOTTETOWN, PEI, C1A 4K8400 APPLEWOOD CRES., SUITE 100VAUGHAN, ON, L4K 0C3WWW.IBSTOREY.CAK. CHAISSONDETAILED ENGINEERINGSTUDY1.01 of 1I. STOREY15-049 P&IDTOWN OF TILLSONBURGDRAWING SHEET NAME15-049 POD15-049 P&ID126-OCT-15ISSUED WITH DES 26-OCT-2015KCCONDENSER WATER TANK (T-1)COMP 1COMP 2COMP 3COMPRESSOR#1150 HPCOMPRESSOR#275 HPCOMPRESSOR#350 HPBRINE PUMP 125 HPBRINE PUMP 230 HPCONDENSER PUMP15 HPUNDERFLOOR PUMP5 HPEVAPORATIVE CONDENSER25 HPMEMORIALRINKCOMMUNITYRINKCOMMUNITYRINKSUB FLOORHEATINGTO/FROMSLAPSHOTPADV-1OIL COOLEROIL COOLEROIL COOLERBRINE HEATERT-3T-2T-5T-4AAAABBBBFIRE BOXCHEMICALTREATMENTFLOORDRAINGLYCOL TANKSCHILLER 1CHILLER 2CHILLER 3TO AMMONIA DIFFUSEROIL COOLINGPUMP SLAPSHOTPADBRAZEDPLATEPARALLELCONDENSERTO/FROM IN FLOORHEATINGLEGENDAMMONIAGLYCOLWATER93
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APPENDIX C
MANUFACTURER’S DATA SHEETS
Note: I.B. Storey Inc. does not have any affiliations with manufacturers, suppliers or representatives and retains absolutely no vested interest with proceeding or not proceeding with any
recommendation. The following sheets are examples/snapshots
ONLY. Full list of the various operating condition specifications
can be provided upon request.
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APPENDIX C-1
REFRIGERATION PLANT CONTROLS
OPTMIZATION
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